FORD ESCAPE 2017

Complete listing of complaints and recalls for this vehicle

2.8K
Complaints
4
Recalls

Complaints & Recalls

2.8K Complaints 4 Recalls

Official Safety Recalls - Important!

4 Recalls

These are official manufacturer recalls ordered by NHTSA for safety defects. If you own this vehicle, contact your dealer immediately for free repairs.

Ford Motor Company
NHTSA Campaign: 22V413000 SAFETY RECALL
2.9M Vehicles Affected
Recall Date: Jun 10, 2022
Safety Issue:

Ford Motor Company (Ford) is recalling certain 2013-2019 Escape, 2013-2018 C-Max, 2013-2016 Fusion, 2013-2021 Transit Connect, and 2015-2018 Edge vehicles. The bushing that attaches the shifter cable to the transmission may degrade or detach.

Potential Risk:
A damaged or missing bushing may prevent the vehicle from shifting into the intended gear, and cause the vehicle to move in an unexpected direction. Additionally, the vehicle may roll after the driver selects the 'Park' position. Either scenario increases the risk of a crash or injury.
FREE Recall Solution:
Dealers will replace the under hood shift bushing and add a protective cap over the shift cable bushing, free of charge. Interim owner notification letters, informing owners of the safety risk, were mailed July 1, 2022. Remedy parts are expected to be available in 4th Quarter 2022. Owner notification letters were mailed October 27, 2022. Owners may contact Ford customer service at 1-866-436-7332. Ford's number for this recall is 22S43.
Additional Details:

Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.nhtsa.gov.

Action Required: Contact your local FORD dealer to schedule your FREE recall repair.
Manufacturer: FORD
Mfg Campaign: 22S43
Notice Date: Oct 27, 2022
Recall Date: Jun 10, 2022
Ford Motor Company
NHTSA Campaign: 16V617000 SAFETY RECALL
18K Vehicles Affected
Recall Date: Aug 24, 2016
Safety Issue:

Ford Motor Company (Ford) is recalling certain model year 2017 Ford Escape Titanium and SE vehicles manufactured October 5, 2015, to May 12, 2016. The settings for the closing-force of the power-operated windows may allow the windows to close on an object such as a body part and injure it before the windows auto-reverse. As such, these vehicles fail to comply with the requirements of Federal Motor Vehicle Safety Standard (FMVSS) number 118, "Power-Operated Window Systems."

Potential Risk:
If a window closes on a body part, it can increase the risk of injury.
FREE Recall Solution:
Ford has notified owners, and dealers will update the power window operating system software, free of charge. The recall began on September 6, 2016. Owners may contact Ford customer service at 1-866-436-7332. Ford's number for this recall is 16C12.
Additional Details:

Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.

Action Required: Contact your local FORD dealer to schedule your FREE recall repair.
Manufacturer: FORD
Mfg Campaign: 16C12
Notice Date: Sep 6, 2016
Recall Date: Aug 24, 2016

Consumer Complaints

2.8K Complaints
Ford Motor Company
Campaign: 11622944 Other
Oct 31, 2024
Defect Description:

ENGINE

Potential Consequences:

Vehicle operated poorly at start up for 10-20 seconds. Check engine light came on. I had limited control with braking and accelerating. If my son was outside, I could have accidentally run him over. The dealership told me that it is a known issue involving coolant leaking into the engine cylinder. This issue can only be rectified by replacing the entire engine, which is not covered by any recalls, warranties, etc. at this time. The dealership printed a Technical Service Bulletin for me 22-2229 "2.0L EcoBoost - Coolant in Cylinders, White Exhaust Smoke And/Or Illuminated MIL". This is a known and documented issue that costs $10,000+ to fix and there is no recall?!?!

Corrective Action:

Vehicle operated poorly at start up for 10-20 seconds. Check engine light came on. I had limited control with braking and accelerating. If my son was outside, I could have accidentally run him over. The dealership told me that it is a known issue involving coolant leaking into the engine cylinder. This issue can only be rectified by replacing the entire engine, which is not covered by any recalls, warranties, etc. at this time. The dealership printed a Technical Service Bulletin for me 22-2229 "2.0L EcoBoost - Coolant in Cylinders, White Exhaust Smoke And/Or Illuminated MIL". This is a known and documented issue that costs $10,000+ to fix and there is no recall?!?!

Additional Notes:

Vehicle operated poorly at start up for 10-20 seconds. Check engine light came on. I had limited control with braking and accelerating. If my son was outside, I could have accidentally run him over. The dealership told me that it is a known issue involving coolant leaking into the engine cylinder. This issue can only be rectified by replacing the entire engine, which is not covered by any recalls, warranties, etc. at this time. The dealership printed a Technical Service Bulletin for me 22-2229 "2.0L EcoBoost - Coolant in Cylinders, White Exhaust Smoke And/Or Illuminated MIL". This is a known and documented issue that costs $10,000+ to fix and there is no recall?!?!

Manufacturer: FORD
Mfg Campaign: 11622944
Notice Date: Oct 31, 2024
Recall Date: Oct 31, 2024
Ford Motor Company
Campaign: 11622680 Other
Oct 30, 2024
Defect Description:

ENGINE

Potential Consequences:

Service engine light came on took to Ford dealer to be checked was told need new engine due to coolant intrusion

Corrective Action:

Service engine light came on took to Ford dealer to be checked was told need new engine due to coolant intrusion

Additional Notes:

Service engine light came on took to Ford dealer to be checked was told need new engine due to coolant intrusion

Manufacturer: FORD
Mfg Campaign: 11622680
Notice Date: Oct 30, 2024
Recall Date: Oct 30, 2024
Ford Motor Company
Campaign: 11622746 Other
Oct 30, 2024
Defect Description:

ENGINE AND ENGINE COOLING

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated that upon coming to a complete stop, the message "Engine Hot" was displayed. The contact stated that while driving from a complete stop, the vehicle failed to exceed 10 MPH. The contact was able to pull over to the side of the road. The vehicle was towed to an independent mechanic, where the contact was referred to the dealer for assistance. The vehicle was towed to the dealer, where it was diagnosed with a misfire in cylinder #1 due to coolant intrusion into the engine. The vehicle was not repaired. The contact related the failure to Ford Campaign Number: 21N12. The manufacturer was notified of the failure and informed the contact that the vehicle was not covered. The manufacturer referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 53,500.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated that upon coming to a complete stop, the message "Engine Hot" was displayed. The contact stated that while driving from a complete stop, the vehicle failed to exceed 10 MPH. The contact was able to pull over to the side of the road. The vehicle was towed to an independent mechanic, where the contact was referred to the dealer for assistance. The vehicle was towed to the dealer, where it was diagnosed with a misfire in cylinder #1 due to coolant intrusion into the engine. The vehicle was not repaired. The contact related the failure to Ford Campaign Number: 21N12. The manufacturer was notified of the failure and informed the contact that the vehicle was not covered. The manufacturer referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 53,500.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated that upon coming to a complete stop, the message "Engine Hot" was displayed. The contact stated that while driving from a complete stop, the vehicle failed to exceed 10 MPH. The contact was able to pull over to the side of the road. The vehicle was towed to an independent mechanic, where the contact was referred to the dealer for assistance. The vehicle was towed to the dealer, where it was diagnosed with a misfire in cylinder #1 due to coolant intrusion into the engine. The vehicle was not repaired. The contact related the failure to Ford Campaign Number: 21N12. The manufacturer was notified of the failure and informed the contact that the vehicle was not covered. The manufacturer referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 53,500.

Manufacturer: FORD
Mfg Campaign: 11622746
Notice Date: Oct 30, 2024
Recall Date: Oct 30, 2024
Ford Motor Company
Campaign: 11622786 Other
Oct 30, 2024
Defect Description:

ENGINE

Potential Consequences:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Corrective Action:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Additional Notes:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Manufacturer: FORD
Mfg Campaign: 11622786
Notice Date: Oct 30, 2024
Recall Date: Oct 30, 2024
Ford Motor Company
Campaign: 11622786 Other
Oct 30, 2024
Defect Description:

POWER TRAIN

Potential Consequences:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Corrective Action:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Additional Notes:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Manufacturer: FORD
Mfg Campaign: 11622786
Notice Date: Oct 30, 2024
Recall Date: Oct 30, 2024
Ford Motor Company
Campaign: 11622786 Other
Oct 30, 2024
Defect Description:

UNKNOWN OR OTHER

Potential Consequences:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Corrective Action:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Additional Notes:

For the past two years I have drove a 2017 ford escape. Over the past two years my car has failed me multiple times My question is for ford motor company. Knowing this is a known issue with escapes…why are they doing nothing to help customers who have had a total engine failure due to manufacturing’s flaws ?

Manufacturer: FORD
Mfg Campaign: 11622786
Notice Date: Oct 30, 2024
Recall Date: Oct 30, 2024
Ford Motor Company
Campaign: 11622549 Other
Oct 29, 2024
Defect Description:

ENGINE AND ENGINE COOLING

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated that white smoke was coming from the exhaust pipe with several warning lights illuminated. The crankshaft position sensor, power control module short circuit sensor, and other warning lights are illuminated. The contact had reset the sensors however, the failure persisted. The contact stated that the coolant was leaking however, there was no location of the leak. The contact stated that driving and then shifting into the park(P), the vehicle went into LIMP Mode. The vehicle was returned to the dealer but was not diagnosed or repaired. The manufacturer was made aware of the failure. The manufacturer had referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 80,000.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated that white smoke was coming from the exhaust pipe with several warning lights illuminated. The crankshaft position sensor, power control module short circuit sensor, and other warning lights are illuminated. The contact had reset the sensors however, the failure persisted. The contact stated that the coolant was leaking however, there was no location of the leak. The contact stated that driving and then shifting into the park(P), the vehicle went into LIMP Mode. The vehicle was returned to the dealer but was not diagnosed or repaired. The manufacturer was made aware of the failure. The manufacturer had referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 80,000.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated that white smoke was coming from the exhaust pipe with several warning lights illuminated. The crankshaft position sensor, power control module short circuit sensor, and other warning lights are illuminated. The contact had reset the sensors however, the failure persisted. The contact stated that the coolant was leaking however, there was no location of the leak. The contact stated that driving and then shifting into the park(P), the vehicle went into LIMP Mode. The vehicle was returned to the dealer but was not diagnosed or repaired. The manufacturer was made aware of the failure. The manufacturer had referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 80,000.

Manufacturer: FORD
Mfg Campaign: 11622549
Notice Date: Oct 29, 2024
Recall Date: Oct 29, 2024
Ford Motor Company
Campaign: 11622549 Other
Oct 29, 2024
Defect Description:

ELECTRICAL SYSTEM

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated that white smoke was coming from the exhaust pipe with several warning lights illuminated. The crankshaft position sensor, power control module short circuit sensor, and other warning lights are illuminated. The contact had reset the sensors however, the failure persisted. The contact stated that the coolant was leaking however, there was no location of the leak. The contact stated that driving and then shifting into the park(P), the vehicle went into LIMP Mode. The vehicle was returned to the dealer but was not diagnosed or repaired. The manufacturer was made aware of the failure. The manufacturer had referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 80,000.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated that white smoke was coming from the exhaust pipe with several warning lights illuminated. The crankshaft position sensor, power control module short circuit sensor, and other warning lights are illuminated. The contact had reset the sensors however, the failure persisted. The contact stated that the coolant was leaking however, there was no location of the leak. The contact stated that driving and then shifting into the park(P), the vehicle went into LIMP Mode. The vehicle was returned to the dealer but was not diagnosed or repaired. The manufacturer was made aware of the failure. The manufacturer had referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 80,000.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated that white smoke was coming from the exhaust pipe with several warning lights illuminated. The crankshaft position sensor, power control module short circuit sensor, and other warning lights are illuminated. The contact had reset the sensors however, the failure persisted. The contact stated that the coolant was leaking however, there was no location of the leak. The contact stated that driving and then shifting into the park(P), the vehicle went into LIMP Mode. The vehicle was returned to the dealer but was not diagnosed or repaired. The manufacturer was made aware of the failure. The manufacturer had referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 80,000.

Manufacturer: FORD
Mfg Campaign: 11622549
Notice Date: Oct 29, 2024
Recall Date: Oct 29, 2024
Ford Motor Company
Campaign: 11622564 Other
Oct 29, 2024
Defect Description:

WHEELS:LUGS/NUTS/BOLTS/STUDS

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated that upon inspection at a local Tire Shop, the contact was informed that the lug nuts on all four wheels were cracked. The contact had 14 lug nuts replaced out-of-pocket; however, there were 6 lug nuts that still needed to be replaced. The vehicle was not repaired. The lug nuts were OEM parts. The manufacturer was not made aware of the failure. The failure mileage was approximately 54,135.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated that upon inspection at a local Tire Shop, the contact was informed that the lug nuts on all four wheels were cracked. The contact had 14 lug nuts replaced out-of-pocket; however, there were 6 lug nuts that still needed to be replaced. The vehicle was not repaired. The lug nuts were OEM parts. The manufacturer was not made aware of the failure. The failure mileage was approximately 54,135.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated that upon inspection at a local Tire Shop, the contact was informed that the lug nuts on all four wheels were cracked. The contact had 14 lug nuts replaced out-of-pocket; however, there were 6 lug nuts that still needed to be replaced. The vehicle was not repaired. The lug nuts were OEM parts. The manufacturer was not made aware of the failure. The failure mileage was approximately 54,135.

Manufacturer: FORD
Mfg Campaign: 11622564
Notice Date: Oct 29, 2024
Recall Date: Oct 29, 2024
Ford Motor Company
Campaign: 11622277 Other
Oct 28, 2024
Defect Description:

ENGINE

Potential Consequences:

Bought vehicle (used 91.5K miles) from Hyundai dealer and on drive home the check engine light illuminated, checked it at home and was P0301 (misfire on cylinder #1). After back and forth with the dealer I agreed to bring in the vehicle for them to diagnose. On the trip to dealer the vehicle overheated and I had to add water and wait roadside before I could continue. At the dealer the problem was diagnosed as coolant leaking into the #1 cylinder at the head gasket (i.e. per TSB 22-2322 and related TSBs) and the fix was a new long block.

Corrective Action:

Bought vehicle (used 91.5K miles) from Hyundai dealer and on drive home the check engine light illuminated, checked it at home and was P0301 (misfire on cylinder #1). After back and forth with the dealer I agreed to bring in the vehicle for them to diagnose. On the trip to dealer the vehicle overheated and I had to add water and wait roadside before I could continue. At the dealer the problem was diagnosed as coolant leaking into the #1 cylinder at the head gasket (i.e. per TSB 22-2322 and related TSBs) and the fix was a new long block.

Additional Notes:

Bought vehicle (used 91.5K miles) from Hyundai dealer and on drive home the check engine light illuminated, checked it at home and was P0301 (misfire on cylinder #1). After back and forth with the dealer I agreed to bring in the vehicle for them to diagnose. On the trip to dealer the vehicle overheated and I had to add water and wait roadside before I could continue. At the dealer the problem was diagnosed as coolant leaking into the #1 cylinder at the head gasket (i.e. per TSB 22-2322 and related TSBs) and the fix was a new long block.

Manufacturer: FORD
Mfg Campaign: 11622277
Notice Date: Oct 28, 2024
Recall Date: Oct 28, 2024
Ford Motor Company
Campaign: 11622280 Other
Oct 28, 2024
Defect Description:

ENGINE

Potential Consequences:

Coolant was leaking into the engine creating a need for a full engine replacement. Signs of the issue included check engine lights appearing on dashboard twice in two weeks and no coolant remaining in the vehicle. This issue has been reported multiple times by other owners of Ford Escapes with no recourse from Ford. Issue was reported to me by an independent car mechanic. Engine is being replaced this week, therefore no receipt for repairs is yet available, but estimate was $9000.

Corrective Action:

Coolant was leaking into the engine creating a need for a full engine replacement. Signs of the issue included check engine lights appearing on dashboard twice in two weeks and no coolant remaining in the vehicle. This issue has been reported multiple times by other owners of Ford Escapes with no recourse from Ford. Issue was reported to me by an independent car mechanic. Engine is being replaced this week, therefore no receipt for repairs is yet available, but estimate was $9000.

Additional Notes:

Coolant was leaking into the engine creating a need for a full engine replacement. Signs of the issue included check engine lights appearing on dashboard twice in two weeks and no coolant remaining in the vehicle. This issue has been reported multiple times by other owners of Ford Escapes with no recourse from Ford. Issue was reported to me by an independent car mechanic. Engine is being replaced this week, therefore no receipt for repairs is yet available, but estimate was $9000.

Manufacturer: FORD
Mfg Campaign: 11622280
Notice Date: Oct 28, 2024
Recall Date: Oct 28, 2024
Ford Motor Company
Campaign: 11622322 Other
Oct 28, 2024
Defect Description:

POWER TRAIN

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated that while at a stop sign, the vehicle stalled. The vehicle was restarted but failed to shift into gear. While driving 55 MPH, the speedometer decreased, the vehicle failed to accelerate and then stalled. The contact was able to veer over to the side of the road. The vehicle failed to shift into gear. There were no warning lights illuminated. The contact called for a tow truck. The tow truck driver informed the contact that there was coolant leaking from the vehicle. The vehicle was towed to an independent mechanic. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was contacted and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 208,000.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated that while at a stop sign, the vehicle stalled. The vehicle was restarted but failed to shift into gear. While driving 55 MPH, the speedometer decreased, the vehicle failed to accelerate and then stalled. The contact was able to veer over to the side of the road. The vehicle failed to shift into gear. There were no warning lights illuminated. The contact called for a tow truck. The tow truck driver informed the contact that there was coolant leaking from the vehicle. The vehicle was towed to an independent mechanic. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was contacted and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 208,000.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated that while at a stop sign, the vehicle stalled. The vehicle was restarted but failed to shift into gear. While driving 55 MPH, the speedometer decreased, the vehicle failed to accelerate and then stalled. The contact was able to veer over to the side of the road. The vehicle failed to shift into gear. There were no warning lights illuminated. The contact called for a tow truck. The tow truck driver informed the contact that there was coolant leaking from the vehicle. The vehicle was towed to an independent mechanic. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was contacted and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 208,000.

Manufacturer: FORD
Mfg Campaign: 11622322
Notice Date: Oct 28, 2024
Recall Date: Oct 28, 2024
Ford Motor Company
Campaign: 11622322 Other
Oct 28, 2024
Defect Description:

ENGINE AND ENGINE COOLING

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated that while at a stop sign, the vehicle stalled. The vehicle was restarted but failed to shift into gear. While driving 55 MPH, the speedometer decreased, the vehicle failed to accelerate and then stalled. The contact was able to veer over to the side of the road. The vehicle failed to shift into gear. There were no warning lights illuminated. The contact called for a tow truck. The tow truck driver informed the contact that there was coolant leaking from the vehicle. The vehicle was towed to an independent mechanic. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was contacted and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 208,000.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated that while at a stop sign, the vehicle stalled. The vehicle was restarted but failed to shift into gear. While driving 55 MPH, the speedometer decreased, the vehicle failed to accelerate and then stalled. The contact was able to veer over to the side of the road. The vehicle failed to shift into gear. There were no warning lights illuminated. The contact called for a tow truck. The tow truck driver informed the contact that there was coolant leaking from the vehicle. The vehicle was towed to an independent mechanic. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was contacted and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 208,000.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated that while at a stop sign, the vehicle stalled. The vehicle was restarted but failed to shift into gear. While driving 55 MPH, the speedometer decreased, the vehicle failed to accelerate and then stalled. The contact was able to veer over to the side of the road. The vehicle failed to shift into gear. There were no warning lights illuminated. The contact called for a tow truck. The tow truck driver informed the contact that there was coolant leaking from the vehicle. The vehicle was towed to an independent mechanic. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was contacted and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 208,000.

Manufacturer: FORD
Mfg Campaign: 11622322
Notice Date: Oct 28, 2024
Recall Date: Oct 28, 2024
Ford Motor Company
Campaign: 11622060 Other
Oct 26, 2024
Defect Description:

ENGINE

Potential Consequences:

My child and I were driving in the car when it suddenly overhead to extreme temperatures. I've only had this car 2 years, come to find out there's a faulty design to the engine cylinders causing coolant to seep in to the engine, also causing the head gasket to blow. This is ford's fault and there's currently class action lawsuits because this can cause the engine to combust, incredibly dangerous. There needs to be recalls

Corrective Action:

My child and I were driving in the car when it suddenly overhead to extreme temperatures. I've only had this car 2 years, come to find out there's a faulty design to the engine cylinders causing coolant to seep in to the engine, also causing the head gasket to blow. This is ford's fault and there's currently class action lawsuits because this can cause the engine to combust, incredibly dangerous. There needs to be recalls

Additional Notes:

My child and I were driving in the car when it suddenly overhead to extreme temperatures. I've only had this car 2 years, come to find out there's a faulty design to the engine cylinders causing coolant to seep in to the engine, also causing the head gasket to blow. This is ford's fault and there's currently class action lawsuits because this can cause the engine to combust, incredibly dangerous. There needs to be recalls

Manufacturer: FORD
Mfg Campaign: 11622060
Notice Date: Oct 26, 2024
Recall Date: Oct 26, 2024
Ford Motor Company
Campaign: 11622086 Other
Oct 26, 2024
Defect Description:

ENGINE

Potential Consequences:

Coolant leaked into the engine according to McCarthy Ford. Located in North Little Rock, AR. The vehicle started smoking pulling out of the garage.

Corrective Action:

Coolant leaked into the engine according to McCarthy Ford. Located in North Little Rock, AR. The vehicle started smoking pulling out of the garage.

Additional Notes:

Coolant leaked into the engine according to McCarthy Ford. Located in North Little Rock, AR. The vehicle started smoking pulling out of the garage.

Manufacturer: FORD
Mfg Campaign: 11622086
Notice Date: Oct 26, 2024
Recall Date: Oct 26, 2024
Ford Motor Company
Campaign: 11621871 Other
Oct 25, 2024
Defect Description:

ENGINE

Potential Consequences:

I was driving home from my second job, when the "check engine" light came on. I thought "no big deal". As i got further along, I noticed a "skip" in the engine. The "skip", or misfire, continued. Several more miles down the road, there was a sudden jolt with the car. A message with an alarm suddenly displayed on my cockpit instrument cluster; " Service Required, See Dealer now". By the time I arrived home, the engine was misfiring quite regularly. I parked the car, called the closest repair shop to set up appointment, and they told me go ahead and bring in car. The car would not restart, so I had car towed to repair shop. The next day, the repair shop called saying vehicle had "Blown Head Gasket " and would take a major repair. The car has not been repaired yet because of the major expense.

Corrective Action:

I was driving home from my second job, when the "check engine" light came on. I thought "no big deal". As i got further along, I noticed a "skip" in the engine. The "skip", or misfire, continued. Several more miles down the road, there was a sudden jolt with the car. A message with an alarm suddenly displayed on my cockpit instrument cluster; " Service Required, See Dealer now". By the time I arrived home, the engine was misfiring quite regularly. I parked the car, called the closest repair shop to set up appointment, and they told me go ahead and bring in car. The car would not restart, so I had car towed to repair shop. The next day, the repair shop called saying vehicle had "Blown Head Gasket " and would take a major repair. The car has not been repaired yet because of the major expense.

Additional Notes:

I was driving home from my second job, when the "check engine" light came on. I thought "no big deal". As i got further along, I noticed a "skip" in the engine. The "skip", or misfire, continued. Several more miles down the road, there was a sudden jolt with the car. A message with an alarm suddenly displayed on my cockpit instrument cluster; " Service Required, See Dealer now". By the time I arrived home, the engine was misfiring quite regularly. I parked the car, called the closest repair shop to set up appointment, and they told me go ahead and bring in car. The car would not restart, so I had car towed to repair shop. The next day, the repair shop called saying vehicle had "Blown Head Gasket " and would take a major repair. The car has not been repaired yet because of the major expense.

Manufacturer: FORD
Mfg Campaign: 11621871
Notice Date: Oct 25, 2024
Recall Date: Oct 25, 2024
Ford Motor Company
Campaign: 11621876 Other
Oct 25, 2024
Defect Description:

ENGINE AND ENGINE COOLING

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated while the vehicle was parked in the garage it was discovered that large amounts of oil had leaked from the engine onto the garage floor. The vehicle was taken to the local mechanic who diagnosed that the engine had been damaged due to coolant intrusion into the engine cylinders. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The local dealer and manufacturer were notified of the failure, but no assistance was offered. The failure mileage was 123,000.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated while the vehicle was parked in the garage it was discovered that large amounts of oil had leaked from the engine onto the garage floor. The vehicle was taken to the local mechanic who diagnosed that the engine had been damaged due to coolant intrusion into the engine cylinders. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The local dealer and manufacturer were notified of the failure, but no assistance was offered. The failure mileage was 123,000.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated while the vehicle was parked in the garage it was discovered that large amounts of oil had leaked from the engine onto the garage floor. The vehicle was taken to the local mechanic who diagnosed that the engine had been damaged due to coolant intrusion into the engine cylinders. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The local dealer and manufacturer were notified of the failure, but no assistance was offered. The failure mileage was 123,000.

Manufacturer: FORD
Mfg Campaign: 11621876
Notice Date: Oct 25, 2024
Recall Date: Oct 25, 2024
Ford Motor Company
Campaign: 11622011 Other
Oct 25, 2024
Defect Description:

ENGINE AND ENGINE COOLING

Potential Consequences:

The contact's mother owns a 2017 Ford Escape. The contact stated while her mother was driving at an undisclosed speed, the driver noticed a significant amount of smoke coming out of the exhaust pipe. The driver drove to the residence. Additionally, the contact stated that the vehicle had experienced difficulty in starting. The check engine warning light was illuminated. The vehicle was taken to an independent mechanic, where it was diagnosed with coolant intrusion into the engine. The mechanic determined that the failure was related to Ford Campaign Number: 21N12. The contact was referred to the manufacturer for assistance. The dealer was not notified of the failure. The manufacturer was notified of the failure and referred the contact to the NHTSA Hotline for assistance. The failure mileage was 25,901.

Corrective Action:

The contact's mother owns a 2017 Ford Escape. The contact stated while her mother was driving at an undisclosed speed, the driver noticed a significant amount of smoke coming out of the exhaust pipe. The driver drove to the residence. Additionally, the contact stated that the vehicle had experienced difficulty in starting. The check engine warning light was illuminated. The vehicle was taken to an independent mechanic, where it was diagnosed with coolant intrusion into the engine. The mechanic determined that the failure was related to Ford Campaign Number: 21N12. The contact was referred to the manufacturer for assistance. The dealer was not notified of the failure. The manufacturer was notified of the failure and referred the contact to the NHTSA Hotline for assistance. The failure mileage was 25,901.

Additional Notes:

The contact's mother owns a 2017 Ford Escape. The contact stated while her mother was driving at an undisclosed speed, the driver noticed a significant amount of smoke coming out of the exhaust pipe. The driver drove to the residence. Additionally, the contact stated that the vehicle had experienced difficulty in starting. The check engine warning light was illuminated. The vehicle was taken to an independent mechanic, where it was diagnosed with coolant intrusion into the engine. The mechanic determined that the failure was related to Ford Campaign Number: 21N12. The contact was referred to the manufacturer for assistance. The dealer was not notified of the failure. The manufacturer was notified of the failure and referred the contact to the NHTSA Hotline for assistance. The failure mileage was 25,901.

Manufacturer: FORD
Mfg Campaign: 11622011
Notice Date: Oct 25, 2024
Recall Date: Oct 25, 2024
Ford Motor Company
Campaign: 11622022 Other
Oct 25, 2024
Defect Description:

ENGINE AND ENGINE COOLING

Potential Consequences:

The contact owns a 2017 Ford Escape. The contact stated while driving 55 MPH, the check engine warning light illuminated. The vehicle was taken to an independent mechanic to be diagnosed. The contact was informed that the ignition coils and spark plugs needed to be replaced. The vehicle was repaired however, the failure recurred, and the vehicle was taken back to the independent mechanic again and the ignition coils were replaced; however, the check engine warning light became illuminated. The contact was informed that there was a coolant leak into cylinder #1. The vehicle was not repaired. The manufacturer was not notified of the failure. The approximate failure mileage was 106,000.

Corrective Action:

The contact owns a 2017 Ford Escape. The contact stated while driving 55 MPH, the check engine warning light illuminated. The vehicle was taken to an independent mechanic to be diagnosed. The contact was informed that the ignition coils and spark plugs needed to be replaced. The vehicle was repaired however, the failure recurred, and the vehicle was taken back to the independent mechanic again and the ignition coils were replaced; however, the check engine warning light became illuminated. The contact was informed that there was a coolant leak into cylinder #1. The vehicle was not repaired. The manufacturer was not notified of the failure. The approximate failure mileage was 106,000.

Additional Notes:

The contact owns a 2017 Ford Escape. The contact stated while driving 55 MPH, the check engine warning light illuminated. The vehicle was taken to an independent mechanic to be diagnosed. The contact was informed that the ignition coils and spark plugs needed to be replaced. The vehicle was repaired however, the failure recurred, and the vehicle was taken back to the independent mechanic again and the ignition coils were replaced; however, the check engine warning light became illuminated. The contact was informed that there was a coolant leak into cylinder #1. The vehicle was not repaired. The manufacturer was not notified of the failure. The approximate failure mileage was 106,000.

Manufacturer: FORD
Mfg Campaign: 11622022
Notice Date: Oct 25, 2024
Recall Date: Oct 25, 2024
Ford Motor Company
Campaign: 11621764 Other
Oct 24, 2024
Defect Description:

ENGINE

Potential Consequences:

The "engine light" came on and reported a misfire in cylinder 3. After further research, I found that this is an indicator of the failure of a gasket allowing coolant to leak into the cylinder causing the misfire. I have had the issue diagnosed, confirming the gasket failure by two garages, one being a Ford dealership. Further research has shown that this is a known flaw to the Ford Company, caused by the engine design. The "fix" is a long block engine replacement. If no action is taken the engine will eventually loose coolant and over heat, or the damage in the cylinder will ultimately cause the engine to lock up, likely causing an accident and thus putting occupants of the SUV and possibly others at risk of injury. My car had approximately 100,000 miles when the issue was first indicated, approximately six months after purchasing the vehicle from a Ford dealership.

Corrective Action:

The "engine light" came on and reported a misfire in cylinder 3. After further research, I found that this is an indicator of the failure of a gasket allowing coolant to leak into the cylinder causing the misfire. I have had the issue diagnosed, confirming the gasket failure by two garages, one being a Ford dealership. Further research has shown that this is a known flaw to the Ford Company, caused by the engine design. The "fix" is a long block engine replacement. If no action is taken the engine will eventually loose coolant and over heat, or the damage in the cylinder will ultimately cause the engine to lock up, likely causing an accident and thus putting occupants of the SUV and possibly others at risk of injury. My car had approximately 100,000 miles when the issue was first indicated, approximately six months after purchasing the vehicle from a Ford dealership.

Additional Notes:

The "engine light" came on and reported a misfire in cylinder 3. After further research, I found that this is an indicator of the failure of a gasket allowing coolant to leak into the cylinder causing the misfire. I have had the issue diagnosed, confirming the gasket failure by two garages, one being a Ford dealership. Further research has shown that this is a known flaw to the Ford Company, caused by the engine design. The "fix" is a long block engine replacement. If no action is taken the engine will eventually loose coolant and over heat, or the damage in the cylinder will ultimately cause the engine to lock up, likely causing an accident and thus putting occupants of the SUV and possibly others at risk of injury. My car had approximately 100,000 miles when the issue was first indicated, approximately six months after purchasing the vehicle from a Ford dealership.

Manufacturer: FORD
Mfg Campaign: 11621764
Notice Date: Oct 24, 2024
Recall Date: Oct 24, 2024

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