Complaints & Recalls
Official Safety Recalls - Important!
15 RecallsThese are official manufacturer recalls ordered by NHTSA for safety defects. If you own this vehicle, contact your dealer immediately for free repairs.
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain 2015-2018 Ford Edge and 2016-2018 Lincoln MKX vehicles. The front brake hoses may rupture prematurely.
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 20S42
Recall Date: Aug 11, 2020
Ford Motor Company
Safety Issue:
Ford Motor Company, Inc. (Ford) is recalling certain 2016-2018 Lincoln MKX and 2019-2020 Nautilus vehicles equipped with 16-way electric tilt seats. The seat cushion frame edge may contact the wire harness when the seat occupant uses the tilt function of the seat, potentially damaging one or more wires within the harness, which can result in either inadvertent deployment of the air bag or nondeployment of the air bag in the event of a crash.
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 20S37
Recall Date: Jul 17, 2020
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain 2016-2017 Lincoln MKX vehicles equipped with 3.7L engines. The battery positive cable harness may contact the transmission shifter cable bracket resulting in a short circuit.
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 19S41
Recall Date: Nov 12, 2019
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain 2013-2016 Ford Fusion and Lincoln MKZ, 2015-2016 Ford Edge, and 2016 Lincoln MKX vehicles originally sold, or currently registered in Connecticut, Delaware, the District of Columbia, Illinois, Indiana, Iowa, Maine, Maryland, Massachusetts, Michigan, Minnesota, Missouri, New Hampshire, New Jersey, New York, Ohio, Pennsylvania, Rhode Island, Vermont, West Virginia, and Wisconsin. Road salt or other contaminants may corrode the electric power steering gear motor attachment bolts.
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 19S26
Recall Date: Aug 29, 2019
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain 2016-2017 Ford Edge and Lincoln MKX vehicles and 2017 Lincoln Continental vehicles. In the event of a crash, the driver's frontal air bag may not fully inflate or the air bag cushion may detach from the air bag module. As such, these vehicles fail to comply with the requirements of Federal Motor Vehicle Safety Standard (FMVSS) number 208, "Occupant Crash Protection."
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 17C02
Recall Date: Feb 27, 2017
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain model year 2016 Lincoln MKX vehicles manufactured September 24, 2015. An incorrect seat back trim cover was installed on the affected vehicles, blocking the child seat tether anchors in the second row center seating position. As such, these vehicles fail to comply with the requirements of Federal Motor Vehicle Safety Standard number 225, "Child restraint anchorage systems."
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 16C09
Recall Date: May 24, 2016
Consumer Complaints
167 ComplaintsFord Motor Company
Defect Description:
SERVICE BRAKES
Potential Consequences:
BRAKES GRAB CAUSING VEHICLE TO SKID ON WET PAVEMENT. PASSENGERS ARE RESTRAINED BY SEAT BELTS AND LOOSE ITEMS IN VEHICLE TOSSED TOWARDS FRONT. WILL HAPPEN UNDER LIGHT PEDAL APPLICATION EVEN WHEN APPLIED KNOWING THE PROBLEM EXITS. HAVE ALMOST SLID OF ROADWAY ON CURVES USING EXTREME CAUTION BRAKING.
Corrective Action:
BRAKES GRAB CAUSING VEHICLE TO SKID ON WET PAVEMENT. PASSENGERS ARE RESTRAINED BY SEAT BELTS AND LOOSE ITEMS IN VEHICLE TOSSED TOWARDS FRONT. WILL HAPPEN UNDER LIGHT PEDAL APPLICATION EVEN WHEN APPLIED KNOWING THE PROBLEM EXITS. HAVE ALMOST SLID OF ROADWAY ON CURVES USING EXTREME CAUTION BRAKING.
Additional Notes:
BRAKES GRAB CAUSING VEHICLE TO SKID ON WET PAVEMENT. PASSENGERS ARE RESTRAINED BY SEAT BELTS AND LOOSE ITEMS IN VEHICLE TOSSED TOWARDS FRONT. WILL HAPPEN UNDER LIGHT PEDAL APPLICATION EVEN WHEN APPLIED KNOWING THE PROBLEM EXITS. HAVE ALMOST SLID OF ROADWAY ON CURVES USING EXTREME CAUTION BRAKING.
Mfg Campaign: 10955205
Recall Date: Feb 17, 2017
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
I HAVE HAD PROBLEMS WITH MY 2016 MKX, PURCHASED IN JUNE OF 2016. THE EXHAUST SYSTEM HAS BEEN LEAKING INTO THE CABIN. I ACTUALLY TOOK THE CAR IN FOR SERVICE, BUT THE CAR DEALERSHIP COULD NOT FIND AN ISSUE. THEY CLEANED UNDERNEATH THE EXHAUST LINES AND IT HAS IMPROVED. THE VEHICLE IS USUALLY IN MOTION, I LIVE IN AN AREA WITH HILLS USUALLY AFTER CLIMBING UP A HILL OF A CITY STREET. I HAVE NOTICED THE SMELL LINGERING EVEN AFTER I'VE BEEN OUT OF THE CAR. I'VE SEEN ON OTHER SITES WHERE OTHER LINCOLN OWNERS HAVE COMPLAINED AS WELL. I'M POSTING THIS MESSAGE AS I BELIEVE THE EXHAUST SYSTEM ISSUE FOR FORD IS BEYOND JUST THE FORD LINE AND ALSO LINCOLN.
Corrective Action:
I HAVE HAD PROBLEMS WITH MY 2016 MKX, PURCHASED IN JUNE OF 2016. THE EXHAUST SYSTEM HAS BEEN LEAKING INTO THE CABIN. I ACTUALLY TOOK THE CAR IN FOR SERVICE, BUT THE CAR DEALERSHIP COULD NOT FIND AN ISSUE. THEY CLEANED UNDERNEATH THE EXHAUST LINES AND IT HAS IMPROVED. THE VEHICLE IS USUALLY IN MOTION, I LIVE IN AN AREA WITH HILLS USUALLY AFTER CLIMBING UP A HILL OF A CITY STREET. I HAVE NOTICED THE SMELL LINGERING EVEN AFTER I'VE BEEN OUT OF THE CAR. I'VE SEEN ON OTHER SITES WHERE OTHER LINCOLN OWNERS HAVE COMPLAINED AS WELL. I'M POSTING THIS MESSAGE AS I BELIEVE THE EXHAUST SYSTEM ISSUE FOR FORD IS BEYOND JUST THE FORD LINE AND ALSO LINCOLN.
Additional Notes:
I HAVE HAD PROBLEMS WITH MY 2016 MKX, PURCHASED IN JUNE OF 2016. THE EXHAUST SYSTEM HAS BEEN LEAKING INTO THE CABIN. I ACTUALLY TOOK THE CAR IN FOR SERVICE, BUT THE CAR DEALERSHIP COULD NOT FIND AN ISSUE. THEY CLEANED UNDERNEATH THE EXHAUST LINES AND IT HAS IMPROVED. THE VEHICLE IS USUALLY IN MOTION, I LIVE IN AN AREA WITH HILLS USUALLY AFTER CLIMBING UP A HILL OF A CITY STREET. I HAVE NOTICED THE SMELL LINGERING EVEN AFTER I'VE BEEN OUT OF THE CAR. I'VE SEEN ON OTHER SITES WHERE OTHER LINCOLN OWNERS HAVE COMPLAINED AS WELL. I'M POSTING THIS MESSAGE AS I BELIEVE THE EXHAUST SYSTEM ISSUE FOR FORD IS BEYOND JUST THE FORD LINE AND ALSO LINCOLN.
Mfg Campaign: 10955176
Recall Date: Feb 16, 2017
Ford Motor Company
Defect Description:
VEHICLE SPEED CONTROL
Potential Consequences:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Corrective Action:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Additional Notes:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Mfg Campaign: 10938359
Recall Date: Dec 28, 2016
Ford Motor Company
Defect Description:
STEERING
Potential Consequences:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Corrective Action:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Additional Notes:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Mfg Campaign: 10938359
Recall Date: Dec 28, 2016
Ford Motor Company
Defect Description:
SUSPENSION
Potential Consequences:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Corrective Action:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Additional Notes:
2016 LINCOLN MKX - FWD- LOSES BALANCE WHEN ACCELERATED. ITS WOBBLES/ SWIRLS WHEN STEPPED ON THE GAS ON A CITY STREET OR ON A HIGHWAY. WHEN WE BROUGHT THE CAR IN, LINCOLN DEALERSHIP SERVICES FOREMAN, ADVISER AND DIRECTOR CLAIMED ITS THEIR MKX FWD NORMAL CHARACTERISTICS. THE DEALERSHIP DID NOT DISCLOSE THIS DEFECTIVE DESIGN AT THE TIME OF PURCHASING. THERE ARE NO FIXES, AND THE MKX AWD DOES NOT HAVE THIS PROBLEM/CHARACTERISTICS. WE HAVE CONTACT THE CORPORATE OFFICE AND THE MANAGER SAID THEY TRUSTED THEIR SERVICES ENGINEERS THAT ITS THE NORMAL CHARACTERISTICS OF THE MKX AWD. BOTH THE ADVISER AND THE CORPORATE MANAGER SAID FOR US TO REPORT TO OUR INSURANCE COMPANY IF WE GOT INTO AN ACCIDENT BECAUSE OF THIS DEFECTIVE DESIGN. WE BOUGHT A VERY EXPENSIVE CAR, BUT UNABLE TO USE ITS ABILITIES, BECAUSE IT IS UNSAFE TO ACCELERATE. WHO WOULD BUY A VERY EXPENSIVE CAR AND AFRAID TO STEP ON THE GAS? LINCOLN NEEDS TO DISCLOSE THE MKX FWD- DEFECTIVE DESIGNS THAT THEY CLAIMED TO BE THE NORMAL CHARACTERISTICS TO THEIR CUSTOMERS AT THE TIME OF BUYING. OR THEY NEED TO STOP PUTTING THE ECO BOOST ENG ON THE FWD MKX CARS.
Mfg Campaign: 10938359
Recall Date: Dec 28, 2016
Ford Motor Company
Defect Description:
FUEL/PROPULSION SYSTEM
Potential Consequences:
IN JULY 2016 I BOUGHT A NEW LINCOLN MKX WITH THE 2.7 ECO ENGINE. FROM DAY ONE I NOTICED FIBERGLASS PARTICLES ON THE REAR GLASS , AFTER 300 MILES IT WAS SO BAD I HAD TO WASH IT EVERY DAY , IT WAS ALSO IN SIDE ALL OVER THE INTERIOR. I HAD IT ON MY FACE AS WELL AS MY FAMILY. I CONTACTED LINCOLN AND THEY DENIED USING FIBERGLASS ON THEIR VEHICLES. LINCOLN TOLD ME TO TAKE IT TO MY DEALER AND I DID AFTER SEVERAL VISITS THEY DISCOVERED IT WAS COMING FROM THE EXHAUST AND CONTACTED LINCOLN . IN THE MEANTIME I STARTED COUGHING AND HAD SEVERE THROAT IRATATION. I STARTED TO CALL LINCOLN CUSTOMER SERVICE BUT AFTER A PERIOD OF TIME WAS TOLD TO STOP CALLING. THE DEALER DID NOT SEEM TO GET ANY WHERE WITH THIS PROBLEM. LINCOLN ADVISED ME TO KEEP THE WINDOWS UP, I REQUESTED A LOANER VEHICLE TILL THE PROBLEM WAS RESOLVED AND WAS TOLD NO BECAUSE THE VEHICLE RAN AND WAS OPERATIONAL THEY COULD NOT DO THIS. AFTER 2800 MILES AND 3 MONTHS OF OWNER SHIP I WAS FORCED TO TRADE IT IN AND TAKE A $18,000.00 DOLLARS LOSS. I WENT TO THE VA HOSPITAL AND WAS TOLD TO STAY AWAY FROM THE MKX AFTER EXAMS BECAUSE FIBERGLASS WILL CAUSE THESE COUGHING AND IRATITAON PROBLEMS, SYMPTOMS I DOCUMENTED THIS ON UTUBE UNDER - [ 2016 LINCOLN MKX PROBLEMS.] BEING A VET AND ON DISABILITY THE LOSS WAS GREAT . I DO FEEL SORRY FOR THE OTHERS THAT ARE EXPERIENCING THIS PROBLEM THIS HAS GOT TO BE THE BIGGEST LOSS I EVER HAD ON AN AUTOMOBILE
Corrective Action:
IN JULY 2016 I BOUGHT A NEW LINCOLN MKX WITH THE 2.7 ECO ENGINE. FROM DAY ONE I NOTICED FIBERGLASS PARTICLES ON THE REAR GLASS , AFTER 300 MILES IT WAS SO BAD I HAD TO WASH IT EVERY DAY , IT WAS ALSO IN SIDE ALL OVER THE INTERIOR. I HAD IT ON MY FACE AS WELL AS MY FAMILY. I CONTACTED LINCOLN AND THEY DENIED USING FIBERGLASS ON THEIR VEHICLES. LINCOLN TOLD ME TO TAKE IT TO MY DEALER AND I DID AFTER SEVERAL VISITS THEY DISCOVERED IT WAS COMING FROM THE EXHAUST AND CONTACTED LINCOLN . IN THE MEANTIME I STARTED COUGHING AND HAD SEVERE THROAT IRATATION. I STARTED TO CALL LINCOLN CUSTOMER SERVICE BUT AFTER A PERIOD OF TIME WAS TOLD TO STOP CALLING. THE DEALER DID NOT SEEM TO GET ANY WHERE WITH THIS PROBLEM. LINCOLN ADVISED ME TO KEEP THE WINDOWS UP, I REQUESTED A LOANER VEHICLE TILL THE PROBLEM WAS RESOLVED AND WAS TOLD NO BECAUSE THE VEHICLE RAN AND WAS OPERATIONAL THEY COULD NOT DO THIS. AFTER 2800 MILES AND 3 MONTHS OF OWNER SHIP I WAS FORCED TO TRADE IT IN AND TAKE A $18,000.00 DOLLARS LOSS. I WENT TO THE VA HOSPITAL AND WAS TOLD TO STAY AWAY FROM THE MKX AFTER EXAMS BECAUSE FIBERGLASS WILL CAUSE THESE COUGHING AND IRATITAON PROBLEMS, SYMPTOMS I DOCUMENTED THIS ON UTUBE UNDER - [ 2016 LINCOLN MKX PROBLEMS.] BEING A VET AND ON DISABILITY THE LOSS WAS GREAT . I DO FEEL SORRY FOR THE OTHERS THAT ARE EXPERIENCING THIS PROBLEM THIS HAS GOT TO BE THE BIGGEST LOSS I EVER HAD ON AN AUTOMOBILE
Additional Notes:
IN JULY 2016 I BOUGHT A NEW LINCOLN MKX WITH THE 2.7 ECO ENGINE. FROM DAY ONE I NOTICED FIBERGLASS PARTICLES ON THE REAR GLASS , AFTER 300 MILES IT WAS SO BAD I HAD TO WASH IT EVERY DAY , IT WAS ALSO IN SIDE ALL OVER THE INTERIOR. I HAD IT ON MY FACE AS WELL AS MY FAMILY. I CONTACTED LINCOLN AND THEY DENIED USING FIBERGLASS ON THEIR VEHICLES. LINCOLN TOLD ME TO TAKE IT TO MY DEALER AND I DID AFTER SEVERAL VISITS THEY DISCOVERED IT WAS COMING FROM THE EXHAUST AND CONTACTED LINCOLN . IN THE MEANTIME I STARTED COUGHING AND HAD SEVERE THROAT IRATATION. I STARTED TO CALL LINCOLN CUSTOMER SERVICE BUT AFTER A PERIOD OF TIME WAS TOLD TO STOP CALLING. THE DEALER DID NOT SEEM TO GET ANY WHERE WITH THIS PROBLEM. LINCOLN ADVISED ME TO KEEP THE WINDOWS UP, I REQUESTED A LOANER VEHICLE TILL THE PROBLEM WAS RESOLVED AND WAS TOLD NO BECAUSE THE VEHICLE RAN AND WAS OPERATIONAL THEY COULD NOT DO THIS. AFTER 2800 MILES AND 3 MONTHS OF OWNER SHIP I WAS FORCED TO TRADE IT IN AND TAKE A $18,000.00 DOLLARS LOSS. I WENT TO THE VA HOSPITAL AND WAS TOLD TO STAY AWAY FROM THE MKX AFTER EXAMS BECAUSE FIBERGLASS WILL CAUSE THESE COUGHING AND IRATITAON PROBLEMS, SYMPTOMS I DOCUMENTED THIS ON UTUBE UNDER - [ 2016 LINCOLN MKX PROBLEMS.] BEING A VET AND ON DISABILITY THE LOSS WAS GREAT . I DO FEEL SORRY FOR THE OTHERS THAT ARE EXPERIENCING THIS PROBLEM THIS HAS GOT TO BE THE BIGGEST LOSS I EVER HAD ON AN AUTOMOBILE
Mfg Campaign: 10937417
Recall Date: Dec 26, 2016
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Corrective Action:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Additional Notes:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Mfg Campaign: 10919890
Recall Date: Oct 28, 2016
Ford Motor Company
Defect Description:
FUEL/PROPULSION SYSTEM
Potential Consequences:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Corrective Action:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Additional Notes:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Mfg Campaign: 10919890
Recall Date: Oct 28, 2016
Ford Motor Company
Defect Description:
VEHICLE SPEED CONTROL
Potential Consequences:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Corrective Action:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Additional Notes:
VEHICLE PURCHASED FEBRUARY 2016. ON MARCH 15, 2016 (1,065 MILES), DRIVING VEHICLE APPROACHING AN INTERSECTION ON A BUSY STREET TO MAKE A LEFT TURN ONTO A MAJOR HIGHWAY ON-RAMP, VEHICLE LOST POWER WHILE IN MOTION AND APPEARED TO ENTER "ACCESSORY MODE". WAS ABLE TO BRING VEHICLE TO STOP (IN THE MIDDLE OF THE INTERSECTION), PUT IT IN PARK AND RESTART THE VEHICLE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. SERVICE DEPARTMENT HAD VEHICLE FOR TWO DAYS AND COULD NOT DIAGNOSE OR REPLICATE THE PROBLEM. GAVE THE VEHICLE BACK TO ME WITHOUT ATTEMPTING ANY REPAIRS. ON MAY 14, 2016 (2,838 MILES), DRIVING AT LOW SPEED ON BACK ROADS, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT COULD NOT REPLICATE THE ISSUE, BUT FOUND A TSB THAT THEY THOUGHT WOULD APPLY TO THE ISSUE. THE TECHNICIANS REPROGRAMMED THE SOFTWARE IN THE POWER CONTROL MODULE AND GAVE THE VEHICLE BACK TO ME. ON JUNE 25, 2016 (3,663 MILES), DRIVING AT LOW SPEED ON A MAIN ROAD, VEHICLE LOST POWER AGAIN WHILE IN MOTION AND ENTERED ACCESSORY MODE. BROUGHT IT IMMEDIATELY TO LINCOLN SERVICE DEPARTMENT. THE SERVICE DEPARTMENT KEPT THE VEHICLE FOR TWO WEEKS TO ATTEMPT TO REPLICATE THE PROBLEM. AFTER SPEAKING WITH LINCOLN CORPORATE ENGINEERS, THE TECHNICIANS REPLACED THE THROTTLE BODY, ASSUMING THAT WAS WHERE THE ISSUE WAS ORIGINATING. LINCOLN REFUSED TO REPLACE THE VEHICLE AND INSISTED THAT THE THROTTLE BODY WAS AT THE BOTTOM OF THE ISSUE. AS OF OCTOBER 28, 2016, THE VEHICLE HAS NOT LOST POWER AGAIN. *TR
Mfg Campaign: 10919890
Recall Date: Oct 28, 2016
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
WHILE DRIVING ON A HIGHWAY IN RUSH HOUR TRAFFIC, MY VEHICLE SUDDENLY LOST ACCELERATION AND WARNING LIGHT/WRENCH SYMBOL CAME ON. I COULD NOT ACCELERATE OVER 10 MPH AND LIMPED TO SIDE OF ROAD. I TURNED OFF VEHICLE FOR ABOUT 20 MINUTES, AFTER THAT TURNED BACK ON AND VEHICLE WORKED COMPLETELY NORMAL. I DROVE TO DEALER IMMEDIATELY, THEY REPLACED THROTTLE BODY AND UPDATED SOFTWARE. MY VEHICLE HAS 10,400 MILES. *TR
Corrective Action:
WHILE DRIVING ON A HIGHWAY IN RUSH HOUR TRAFFIC, MY VEHICLE SUDDENLY LOST ACCELERATION AND WARNING LIGHT/WRENCH SYMBOL CAME ON. I COULD NOT ACCELERATE OVER 10 MPH AND LIMPED TO SIDE OF ROAD. I TURNED OFF VEHICLE FOR ABOUT 20 MINUTES, AFTER THAT TURNED BACK ON AND VEHICLE WORKED COMPLETELY NORMAL. I DROVE TO DEALER IMMEDIATELY, THEY REPLACED THROTTLE BODY AND UPDATED SOFTWARE. MY VEHICLE HAS 10,400 MILES. *TR
Additional Notes:
WHILE DRIVING ON A HIGHWAY IN RUSH HOUR TRAFFIC, MY VEHICLE SUDDENLY LOST ACCELERATION AND WARNING LIGHT/WRENCH SYMBOL CAME ON. I COULD NOT ACCELERATE OVER 10 MPH AND LIMPED TO SIDE OF ROAD. I TURNED OFF VEHICLE FOR ABOUT 20 MINUTES, AFTER THAT TURNED BACK ON AND VEHICLE WORKED COMPLETELY NORMAL. I DROVE TO DEALER IMMEDIATELY, THEY REPLACED THROTTLE BODY AND UPDATED SOFTWARE. MY VEHICLE HAS 10,400 MILES. *TR
Mfg Campaign: 10917221
Recall Date: Oct 18, 2016
Ford Motor Company
Defect Description:
POWER TRAIN
Potential Consequences:
WHILE DRIVING ON A HIGHWAY IN RUSH HOUR TRAFFIC, MY VEHICLE SUDDENLY LOST ACCELERATION AND WARNING LIGHT/WRENCH SYMBOL CAME ON. I COULD NOT ACCELERATE OVER 10 MPH AND LIMPED TO SIDE OF ROAD. I TURNED OFF VEHICLE FOR ABOUT 20 MINUTES, AFTER THAT TURNED BACK ON AND VEHICLE WORKED COMPLETELY NORMAL. I DROVE TO DEALER IMMEDIATELY, THEY REPLACED THROTTLE BODY AND UPDATED SOFTWARE. MY VEHICLE HAS 10,400 MILES. *TR
Corrective Action:
WHILE DRIVING ON A HIGHWAY IN RUSH HOUR TRAFFIC, MY VEHICLE SUDDENLY LOST ACCELERATION AND WARNING LIGHT/WRENCH SYMBOL CAME ON. I COULD NOT ACCELERATE OVER 10 MPH AND LIMPED TO SIDE OF ROAD. I TURNED OFF VEHICLE FOR ABOUT 20 MINUTES, AFTER THAT TURNED BACK ON AND VEHICLE WORKED COMPLETELY NORMAL. I DROVE TO DEALER IMMEDIATELY, THEY REPLACED THROTTLE BODY AND UPDATED SOFTWARE. MY VEHICLE HAS 10,400 MILES. *TR
Additional Notes:
WHILE DRIVING ON A HIGHWAY IN RUSH HOUR TRAFFIC, MY VEHICLE SUDDENLY LOST ACCELERATION AND WARNING LIGHT/WRENCH SYMBOL CAME ON. I COULD NOT ACCELERATE OVER 10 MPH AND LIMPED TO SIDE OF ROAD. I TURNED OFF VEHICLE FOR ABOUT 20 MINUTES, AFTER THAT TURNED BACK ON AND VEHICLE WORKED COMPLETELY NORMAL. I DROVE TO DEALER IMMEDIATELY, THEY REPLACED THROTTLE BODY AND UPDATED SOFTWARE. MY VEHICLE HAS 10,400 MILES. *TR
Mfg Campaign: 10917221
Recall Date: Oct 18, 2016
Ford Motor Company
Defect Description:
VEHICLE SPEED CONTROL
Potential Consequences:
I WAS DRIVING TO MY SON'S HOUSE WHEN THE CAR LOST POWER THERE WAS A CHIME WARNING AND ON THE DASH A MENU STARTING THE HILL ASSIST WAS NOT AVAILABLE THE ENGINE CONTINUE TO RUN BUT THERE WAS NO RESPONSE WHEN I PRESSED ON THE ACCELERATOR THE CAR WOULD ONLY DUE ABOUT 3 MILES AT IDLE SPEED. WAS ABLE RESTART IT AND MAKE BACK HOME, ON THE NEXT DAY10/09/16 I HAD THE SAME PROBLEM THIS TIME I COULD NOT GET IT TO ACCELERATE I HAD THE CAR TOWED TO THE DEALERSHIP IT WAS SUNDAY THE DEALER WAS CLOSED. I CALLED THE DEALER ON MONDAY AND TOLD HIM WHAT HAPPEN AND HE SAID THEY WERE WORKING ON IT. THEY CALLED LATER AND SAID IT WAS THROTTLE CONTROL AND A COUPLE OF ERROR CODES THAT REQUIRED UP DATING P2111, U0415 AND U0416. THEY ALSO REPLACED THE THROTTLE BODY. THEY ALSO NOTED THEY DROVE IT 9 MILES AND NOTED THAT ALL OK AT THIS TIME. THAT LAST COMMENT SOUNDS THAT THIS COULD HAPPEN AGAIN. THIS IS A VERY DANGEROUS PROBLEM HAD I BEEN ON THE INTERSTATE AT RUSH HOUR I MIGHT NOT BE WRITING THIS TO COMPLAIN. WHEN THIS HAPPENS THE CAR SLOWS ON SO FAST THAT THE CAR BEHIND DOESN'T KNOW YOU HAVE A PROBLEM BECAUSE YOU ARE NOT BRAKING WHICH MEANS YOUR BRAKE LIGHTS ARE NOT ON AND HE MORE THAN LIKELY IS GOING TO HIT YOU. THE FIRST TIME THIS HAPPENS IS QUIET SCARY BECAUSE YOU HAVE NO IDEA WHAT IS HAPPENING.
Corrective Action:
I WAS DRIVING TO MY SON'S HOUSE WHEN THE CAR LOST POWER THERE WAS A CHIME WARNING AND ON THE DASH A MENU STARTING THE HILL ASSIST WAS NOT AVAILABLE THE ENGINE CONTINUE TO RUN BUT THERE WAS NO RESPONSE WHEN I PRESSED ON THE ACCELERATOR THE CAR WOULD ONLY DUE ABOUT 3 MILES AT IDLE SPEED. WAS ABLE RESTART IT AND MAKE BACK HOME, ON THE NEXT DAY10/09/16 I HAD THE SAME PROBLEM THIS TIME I COULD NOT GET IT TO ACCELERATE I HAD THE CAR TOWED TO THE DEALERSHIP IT WAS SUNDAY THE DEALER WAS CLOSED. I CALLED THE DEALER ON MONDAY AND TOLD HIM WHAT HAPPEN AND HE SAID THEY WERE WORKING ON IT. THEY CALLED LATER AND SAID IT WAS THROTTLE CONTROL AND A COUPLE OF ERROR CODES THAT REQUIRED UP DATING P2111, U0415 AND U0416. THEY ALSO REPLACED THE THROTTLE BODY. THEY ALSO NOTED THEY DROVE IT 9 MILES AND NOTED THAT ALL OK AT THIS TIME. THAT LAST COMMENT SOUNDS THAT THIS COULD HAPPEN AGAIN. THIS IS A VERY DANGEROUS PROBLEM HAD I BEEN ON THE INTERSTATE AT RUSH HOUR I MIGHT NOT BE WRITING THIS TO COMPLAIN. WHEN THIS HAPPENS THE CAR SLOWS ON SO FAST THAT THE CAR BEHIND DOESN'T KNOW YOU HAVE A PROBLEM BECAUSE YOU ARE NOT BRAKING WHICH MEANS YOUR BRAKE LIGHTS ARE NOT ON AND HE MORE THAN LIKELY IS GOING TO HIT YOU. THE FIRST TIME THIS HAPPENS IS QUIET SCARY BECAUSE YOU HAVE NO IDEA WHAT IS HAPPENING.
Additional Notes:
I WAS DRIVING TO MY SON'S HOUSE WHEN THE CAR LOST POWER THERE WAS A CHIME WARNING AND ON THE DASH A MENU STARTING THE HILL ASSIST WAS NOT AVAILABLE THE ENGINE CONTINUE TO RUN BUT THERE WAS NO RESPONSE WHEN I PRESSED ON THE ACCELERATOR THE CAR WOULD ONLY DUE ABOUT 3 MILES AT IDLE SPEED. WAS ABLE RESTART IT AND MAKE BACK HOME, ON THE NEXT DAY10/09/16 I HAD THE SAME PROBLEM THIS TIME I COULD NOT GET IT TO ACCELERATE I HAD THE CAR TOWED TO THE DEALERSHIP IT WAS SUNDAY THE DEALER WAS CLOSED. I CALLED THE DEALER ON MONDAY AND TOLD HIM WHAT HAPPEN AND HE SAID THEY WERE WORKING ON IT. THEY CALLED LATER AND SAID IT WAS THROTTLE CONTROL AND A COUPLE OF ERROR CODES THAT REQUIRED UP DATING P2111, U0415 AND U0416. THEY ALSO REPLACED THE THROTTLE BODY. THEY ALSO NOTED THEY DROVE IT 9 MILES AND NOTED THAT ALL OK AT THIS TIME. THAT LAST COMMENT SOUNDS THAT THIS COULD HAPPEN AGAIN. THIS IS A VERY DANGEROUS PROBLEM HAD I BEEN ON THE INTERSTATE AT RUSH HOUR I MIGHT NOT BE WRITING THIS TO COMPLAIN. WHEN THIS HAPPENS THE CAR SLOWS ON SO FAST THAT THE CAR BEHIND DOESN'T KNOW YOU HAVE A PROBLEM BECAUSE YOU ARE NOT BRAKING WHICH MEANS YOUR BRAKE LIGHTS ARE NOT ON AND HE MORE THAN LIKELY IS GOING TO HIT YOU. THE FIRST TIME THIS HAPPENS IS QUIET SCARY BECAUSE YOU HAVE NO IDEA WHAT IS HAPPENING.
Mfg Campaign: 10915740
Recall Date: Oct 13, 2016
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
MY HUSBAND AND I WERE ALMOST KILLED IN THE FAST LANE ON THE INTERSTATE WHEN OUR 2016 LINCOLN MKX SHUT DOWN COMPLETELY, WE HAD TO CROSS THREE LANES OF TRAFFIC WHEN IT STARTED AGAIN ONLY TO SHUT DOWN AGAIN, WE WERE TERRIFIED, IT WAS TOWED TO THE DEALERSHIP WHERE A RECALL WAS JUST ISSUED ON IT CALLED "THROTTLE BODY REPAIR" I ASKED THE SERVICE MANAGER TO REPLACE THIS DEFECTIVE PART , NOT REPAIR IT AND HE DID SO. OUR SERVICE MANAGER WAS PROACTIVE IN THIS AND I PRAY TO GOD WE NEVER EXPERIENCE THIS TYPE OF SITUATION AGAIN. !
Corrective Action:
MY HUSBAND AND I WERE ALMOST KILLED IN THE FAST LANE ON THE INTERSTATE WHEN OUR 2016 LINCOLN MKX SHUT DOWN COMPLETELY, WE HAD TO CROSS THREE LANES OF TRAFFIC WHEN IT STARTED AGAIN ONLY TO SHUT DOWN AGAIN, WE WERE TERRIFIED, IT WAS TOWED TO THE DEALERSHIP WHERE A RECALL WAS JUST ISSUED ON IT CALLED "THROTTLE BODY REPAIR" I ASKED THE SERVICE MANAGER TO REPLACE THIS DEFECTIVE PART , NOT REPAIR IT AND HE DID SO. OUR SERVICE MANAGER WAS PROACTIVE IN THIS AND I PRAY TO GOD WE NEVER EXPERIENCE THIS TYPE OF SITUATION AGAIN. !
Additional Notes:
MY HUSBAND AND I WERE ALMOST KILLED IN THE FAST LANE ON THE INTERSTATE WHEN OUR 2016 LINCOLN MKX SHUT DOWN COMPLETELY, WE HAD TO CROSS THREE LANES OF TRAFFIC WHEN IT STARTED AGAIN ONLY TO SHUT DOWN AGAIN, WE WERE TERRIFIED, IT WAS TOWED TO THE DEALERSHIP WHERE A RECALL WAS JUST ISSUED ON IT CALLED "THROTTLE BODY REPAIR" I ASKED THE SERVICE MANAGER TO REPLACE THIS DEFECTIVE PART , NOT REPAIR IT AND HE DID SO. OUR SERVICE MANAGER WAS PROACTIVE IN THIS AND I PRAY TO GOD WE NEVER EXPERIENCE THIS TYPE OF SITUATION AGAIN. !
Mfg Campaign: 10910708
Recall Date: Sep 30, 2016
Ford Motor Company
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
ON 3 SEPARATE OCCASIONS (MOST RECENT ON 9/16/16) POWER TO VEHICLE SIMPLY CUTS OUT - ON TWO OCCASIONS IT HAS OCCURRED AT HIGH SPEEDS ON BUSY INTERSTATE WITH HEAVY TRAFFIC. EXTREME DANGER, AS UNABLE TO TIMELY PULL TO SIDE OF THE ROAD CAUSING TRAFFIC JAMS AND POTENTIAL ACCIDENTS/REAR-ENDS. SELLING DEALER HAS BEEN UNABLE TO RESOLVE OR FIX PROBLEM.
Corrective Action:
ON 3 SEPARATE OCCASIONS (MOST RECENT ON 9/16/16) POWER TO VEHICLE SIMPLY CUTS OUT - ON TWO OCCASIONS IT HAS OCCURRED AT HIGH SPEEDS ON BUSY INTERSTATE WITH HEAVY TRAFFIC. EXTREME DANGER, AS UNABLE TO TIMELY PULL TO SIDE OF THE ROAD CAUSING TRAFFIC JAMS AND POTENTIAL ACCIDENTS/REAR-ENDS. SELLING DEALER HAS BEEN UNABLE TO RESOLVE OR FIX PROBLEM.
Additional Notes:
ON 3 SEPARATE OCCASIONS (MOST RECENT ON 9/16/16) POWER TO VEHICLE SIMPLY CUTS OUT - ON TWO OCCASIONS IT HAS OCCURRED AT HIGH SPEEDS ON BUSY INTERSTATE WITH HEAVY TRAFFIC. EXTREME DANGER, AS UNABLE TO TIMELY PULL TO SIDE OF THE ROAD CAUSING TRAFFIC JAMS AND POTENTIAL ACCIDENTS/REAR-ENDS. SELLING DEALER HAS BEEN UNABLE TO RESOLVE OR FIX PROBLEM.
Mfg Campaign: 10907519
Recall Date: Sep 19, 2016
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
ON 3 SEPARATE OCCASIONS (MOST RECENT ON 9/16/16) POWER TO VEHICLE SIMPLY CUTS OUT - ON TWO OCCASIONS IT HAS OCCURRED AT HIGH SPEEDS ON BUSY INTERSTATE WITH HEAVY TRAFFIC. EXTREME DANGER, AS UNABLE TO TIMELY PULL TO SIDE OF THE ROAD CAUSING TRAFFIC JAMS AND POTENTIAL ACCIDENTS/REAR-ENDS. SELLING DEALER HAS BEEN UNABLE TO RESOLVE OR FIX PROBLEM.
Corrective Action:
ON 3 SEPARATE OCCASIONS (MOST RECENT ON 9/16/16) POWER TO VEHICLE SIMPLY CUTS OUT - ON TWO OCCASIONS IT HAS OCCURRED AT HIGH SPEEDS ON BUSY INTERSTATE WITH HEAVY TRAFFIC. EXTREME DANGER, AS UNABLE TO TIMELY PULL TO SIDE OF THE ROAD CAUSING TRAFFIC JAMS AND POTENTIAL ACCIDENTS/REAR-ENDS. SELLING DEALER HAS BEEN UNABLE TO RESOLVE OR FIX PROBLEM.
Additional Notes:
ON 3 SEPARATE OCCASIONS (MOST RECENT ON 9/16/16) POWER TO VEHICLE SIMPLY CUTS OUT - ON TWO OCCASIONS IT HAS OCCURRED AT HIGH SPEEDS ON BUSY INTERSTATE WITH HEAVY TRAFFIC. EXTREME DANGER, AS UNABLE TO TIMELY PULL TO SIDE OF THE ROAD CAUSING TRAFFIC JAMS AND POTENTIAL ACCIDENTS/REAR-ENDS. SELLING DEALER HAS BEEN UNABLE TO RESOLVE OR FIX PROBLEM.
Mfg Campaign: 10907519
Recall Date: Sep 19, 2016
Ford Motor Company
Defect Description:
FUEL/PROPULSION SYSTEM
Potential Consequences:
I WAS DRIVING IN THE CENTER LANE ON THE BROOKLYN QUEENS EXPRESSWAY TRAVELING HOME FROM ASTORIA, QUEENS TO MY HOME IN BROOKLYN. HAVING PASSED THE ATLANTIC AVENUE EXIT AT APPROXIMATELY 3:15 PM AND PRESSING ON THE GAS PEDAL, THE CAR LOST ACCELERATION AND NO MATTER HOW MUCH I PRESSED THE GAS PEDAL THE CAR COULD ONLY GO ABOUT 10 MILES AN HOUR. THE BQE AT THIS POINT HAS NO SHOULDER TO PULL OVER IN. BY SOME SAVING GRACE, I WAS ABLE TO GLIDE OFF AT THE HAMILTON AVENUE EXIT. THE LINCOLN TOW ARRIVED AT APPROXIMATELY 5:30PM. THE DEALERSHIP'S SERVICE CLOSED AT 5:30 SO I WAS TOWED HOME. THE NEXT MORNING, WEDNESDAY, AUGUST 31 I CALLED LINCOLN FOR A TOW TO THE DEALERSHIP (DANA FORD, STATEN ISLAND) THAT LEASED THE CAR TO ME. THE LINCOLN SERVICE MANAGER, ANTHONY FALLACARO, ASSISTED ME. HE EXPLAINED IT WAS THE THROTTLE BODY AND MOTOR WHICH WERE DEFECTIVE AND MANY CONSUMERS HAVE HAD PROBLEMS. MY MILEAGE AT THIS POINT WAS 2307 MILES, QUITE LOW FOR EIGHT MONTHS OF OWNERSHIP. HOWEVER, FORD/LINCOLN HAS NOT ISSUED A RECALL. YET, THEY HAD TO MAKE NECESSARY ADJUSTMENTS TO THE NEW PART BECAUSE INSTALLING THE SAME PART WOULD CONTINUE TO CAUSE PROBLEMS. I CALLED LINCOLN ON WEDNESDAY, AUGUST 31 2016 AND SPOKE TO MELISSA AND FORMALLY LOGGED A COMPLAINT (CAS - 10455614-D7Z7N8). I EXPRESSED THAT THIS SHOULD NOT HAVE HAPPENED TO A NEW CAR, I LOST CONFIDENCE IN DRIVING THIS CAR AND AM STUCK WITH IT FOR THE REMAINDER OF THE LEASE.
Corrective Action:
I WAS DRIVING IN THE CENTER LANE ON THE BROOKLYN QUEENS EXPRESSWAY TRAVELING HOME FROM ASTORIA, QUEENS TO MY HOME IN BROOKLYN. HAVING PASSED THE ATLANTIC AVENUE EXIT AT APPROXIMATELY 3:15 PM AND PRESSING ON THE GAS PEDAL, THE CAR LOST ACCELERATION AND NO MATTER HOW MUCH I PRESSED THE GAS PEDAL THE CAR COULD ONLY GO ABOUT 10 MILES AN HOUR. THE BQE AT THIS POINT HAS NO SHOULDER TO PULL OVER IN. BY SOME SAVING GRACE, I WAS ABLE TO GLIDE OFF AT THE HAMILTON AVENUE EXIT. THE LINCOLN TOW ARRIVED AT APPROXIMATELY 5:30PM. THE DEALERSHIP'S SERVICE CLOSED AT 5:30 SO I WAS TOWED HOME. THE NEXT MORNING, WEDNESDAY, AUGUST 31 I CALLED LINCOLN FOR A TOW TO THE DEALERSHIP (DANA FORD, STATEN ISLAND) THAT LEASED THE CAR TO ME. THE LINCOLN SERVICE MANAGER, ANTHONY FALLACARO, ASSISTED ME. HE EXPLAINED IT WAS THE THROTTLE BODY AND MOTOR WHICH WERE DEFECTIVE AND MANY CONSUMERS HAVE HAD PROBLEMS. MY MILEAGE AT THIS POINT WAS 2307 MILES, QUITE LOW FOR EIGHT MONTHS OF OWNERSHIP. HOWEVER, FORD/LINCOLN HAS NOT ISSUED A RECALL. YET, THEY HAD TO MAKE NECESSARY ADJUSTMENTS TO THE NEW PART BECAUSE INSTALLING THE SAME PART WOULD CONTINUE TO CAUSE PROBLEMS. I CALLED LINCOLN ON WEDNESDAY, AUGUST 31 2016 AND SPOKE TO MELISSA AND FORMALLY LOGGED A COMPLAINT (CAS - 10455614-D7Z7N8). I EXPRESSED THAT THIS SHOULD NOT HAVE HAPPENED TO A NEW CAR, I LOST CONFIDENCE IN DRIVING THIS CAR AND AM STUCK WITH IT FOR THE REMAINDER OF THE LEASE.
Additional Notes:
I WAS DRIVING IN THE CENTER LANE ON THE BROOKLYN QUEENS EXPRESSWAY TRAVELING HOME FROM ASTORIA, QUEENS TO MY HOME IN BROOKLYN. HAVING PASSED THE ATLANTIC AVENUE EXIT AT APPROXIMATELY 3:15 PM AND PRESSING ON THE GAS PEDAL, THE CAR LOST ACCELERATION AND NO MATTER HOW MUCH I PRESSED THE GAS PEDAL THE CAR COULD ONLY GO ABOUT 10 MILES AN HOUR. THE BQE AT THIS POINT HAS NO SHOULDER TO PULL OVER IN. BY SOME SAVING GRACE, I WAS ABLE TO GLIDE OFF AT THE HAMILTON AVENUE EXIT. THE LINCOLN TOW ARRIVED AT APPROXIMATELY 5:30PM. THE DEALERSHIP'S SERVICE CLOSED AT 5:30 SO I WAS TOWED HOME. THE NEXT MORNING, WEDNESDAY, AUGUST 31 I CALLED LINCOLN FOR A TOW TO THE DEALERSHIP (DANA FORD, STATEN ISLAND) THAT LEASED THE CAR TO ME. THE LINCOLN SERVICE MANAGER, ANTHONY FALLACARO, ASSISTED ME. HE EXPLAINED IT WAS THE THROTTLE BODY AND MOTOR WHICH WERE DEFECTIVE AND MANY CONSUMERS HAVE HAD PROBLEMS. MY MILEAGE AT THIS POINT WAS 2307 MILES, QUITE LOW FOR EIGHT MONTHS OF OWNERSHIP. HOWEVER, FORD/LINCOLN HAS NOT ISSUED A RECALL. YET, THEY HAD TO MAKE NECESSARY ADJUSTMENTS TO THE NEW PART BECAUSE INSTALLING THE SAME PART WOULD CONTINUE TO CAUSE PROBLEMS. I CALLED LINCOLN ON WEDNESDAY, AUGUST 31 2016 AND SPOKE TO MELISSA AND FORMALLY LOGGED A COMPLAINT (CAS - 10455614-D7Z7N8). I EXPRESSED THAT THIS SHOULD NOT HAVE HAPPENED TO A NEW CAR, I LOST CONFIDENCE IN DRIVING THIS CAR AND AM STUCK WITH IT FOR THE REMAINDER OF THE LEASE.
Mfg Campaign: 10906061
Recall Date: Sep 13, 2016
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
LOST POWER WHILE IN MOTION ON CITY STREET, BEGAN RUNNING ROUGH. 'POWERTRAIN' INDICATOR (WRENCH) LIT ON DASH. LIMPED CAR TO PARKING LOT. CALLED SELLING DEALER. CAR TOWED TO DEALER. DEALER REPLACED AIR INTAKE THROTTLE BODY ON WARRENTY. MILEAGE ON CAR 4052. PRODUCTION DATE ON CAR IS 07DEC15, 3.7L V6 ENGINE.
Corrective Action:
LOST POWER WHILE IN MOTION ON CITY STREET, BEGAN RUNNING ROUGH. 'POWERTRAIN' INDICATOR (WRENCH) LIT ON DASH. LIMPED CAR TO PARKING LOT. CALLED SELLING DEALER. CAR TOWED TO DEALER. DEALER REPLACED AIR INTAKE THROTTLE BODY ON WARRENTY. MILEAGE ON CAR 4052. PRODUCTION DATE ON CAR IS 07DEC15, 3.7L V6 ENGINE.
Additional Notes:
LOST POWER WHILE IN MOTION ON CITY STREET, BEGAN RUNNING ROUGH. 'POWERTRAIN' INDICATOR (WRENCH) LIT ON DASH. LIMPED CAR TO PARKING LOT. CALLED SELLING DEALER. CAR TOWED TO DEALER. DEALER REPLACED AIR INTAKE THROTTLE BODY ON WARRENTY. MILEAGE ON CAR 4052. PRODUCTION DATE ON CAR IS 07DEC15, 3.7L V6 ENGINE.
Mfg Campaign: 10906203
Recall Date: Sep 13, 2016
Ford Motor Company
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. WHILE DRIVING APPROXIMATELY 55 MPH, THE VEHICLE LOST POWER AND FAILED TO RESTART. THE ALL WHEEL DRIVE INDICATOR ILLUMINATED. THE CONTACT CALLED FOR ROADSIDE ASSISTANCE, BUT THE VEHICLE RESTARTED BEFORE THEY ARRIVED. THE FAILURE RECURRED ON THE WAY TO THE DEALER, BUT THE VEHICLE RESTARTED. THE DEALER WAS UNABLE TO DUPLICATE THE FAILURE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND INFORMED THE CONTACT TO DOCUMENT WHAT HAPPENED. THE FAILURE MILEAGE WAS 4,500.
Corrective Action:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. WHILE DRIVING APPROXIMATELY 55 MPH, THE VEHICLE LOST POWER AND FAILED TO RESTART. THE ALL WHEEL DRIVE INDICATOR ILLUMINATED. THE CONTACT CALLED FOR ROADSIDE ASSISTANCE, BUT THE VEHICLE RESTARTED BEFORE THEY ARRIVED. THE FAILURE RECURRED ON THE WAY TO THE DEALER, BUT THE VEHICLE RESTARTED. THE DEALER WAS UNABLE TO DUPLICATE THE FAILURE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND INFORMED THE CONTACT TO DOCUMENT WHAT HAPPENED. THE FAILURE MILEAGE WAS 4,500.
Additional Notes:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. WHILE DRIVING APPROXIMATELY 55 MPH, THE VEHICLE LOST POWER AND FAILED TO RESTART. THE ALL WHEEL DRIVE INDICATOR ILLUMINATED. THE CONTACT CALLED FOR ROADSIDE ASSISTANCE, BUT THE VEHICLE RESTARTED BEFORE THEY ARRIVED. THE FAILURE RECURRED ON THE WAY TO THE DEALER, BUT THE VEHICLE RESTARTED. THE DEALER WAS UNABLE TO DUPLICATE THE FAILURE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND INFORMED THE CONTACT TO DOCUMENT WHAT HAPPENED. THE FAILURE MILEAGE WAS 4,500.
Mfg Campaign: 10904632
Recall Date: Sep 8, 2016
Ford Motor Company
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT STATED THAT THE WARNING INDICATOR ILLUMINATED TO CHECK THE HEAD LAMP SYSTEM AND "SEE MANUAL ON THE DISPLAY" DISPLAYED ON THE MESSAGE BOARD. THE VEHICLE WAS TAKEN TO THE DEALER TWICE, BUT THEY WERE UNABLE TO REPLICATE AND DIAGNOSE THE FAILURE. THE DEALER REPROGRAMMED THE HCM, BUT THE WARNING INDICATOR FLASHED SEVERAL TIMES AGAIN MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER A THIRD TIME FOR FURTHER TESTING AGAIN AND THEY LATER TOLD THE CONTACT TO PICK UP THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED. THE CONTACT WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER. THE APPROXIMATE FAILURE MILEAGE WAS 365.
Corrective Action:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT STATED THAT THE WARNING INDICATOR ILLUMINATED TO CHECK THE HEAD LAMP SYSTEM AND "SEE MANUAL ON THE DISPLAY" DISPLAYED ON THE MESSAGE BOARD. THE VEHICLE WAS TAKEN TO THE DEALER TWICE, BUT THEY WERE UNABLE TO REPLICATE AND DIAGNOSE THE FAILURE. THE DEALER REPROGRAMMED THE HCM, BUT THE WARNING INDICATOR FLASHED SEVERAL TIMES AGAIN MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER A THIRD TIME FOR FURTHER TESTING AGAIN AND THEY LATER TOLD THE CONTACT TO PICK UP THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED. THE CONTACT WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER. THE APPROXIMATE FAILURE MILEAGE WAS 365.
Additional Notes:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT STATED THAT THE WARNING INDICATOR ILLUMINATED TO CHECK THE HEAD LAMP SYSTEM AND "SEE MANUAL ON THE DISPLAY" DISPLAYED ON THE MESSAGE BOARD. THE VEHICLE WAS TAKEN TO THE DEALER TWICE, BUT THEY WERE UNABLE TO REPLICATE AND DIAGNOSE THE FAILURE. THE DEALER REPROGRAMMED THE HCM, BUT THE WARNING INDICATOR FLASHED SEVERAL TIMES AGAIN MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER A THIRD TIME FOR FURTHER TESTING AGAIN AND THEY LATER TOLD THE CONTACT TO PICK UP THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED. THE CONTACT WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER. THE APPROXIMATE FAILURE MILEAGE WAS 365.
Mfg Campaign: 10904708
Recall Date: Sep 8, 2016
Ford Motor Company
Defect Description:
EXTERIOR LIGHTING
Potential Consequences:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT STATED THAT THE WARNING INDICATOR ILLUMINATED TO CHECK THE HEAD LAMP SYSTEM AND "SEE MANUAL ON THE DISPLAY" DISPLAYED ON THE MESSAGE BOARD. THE VEHICLE WAS TAKEN TO THE DEALER TWICE, BUT THEY WERE UNABLE TO REPLICATE AND DIAGNOSE THE FAILURE. THE DEALER REPROGRAMMED THE HCM, BUT THE WARNING INDICATOR FLASHED SEVERAL TIMES AGAIN MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER A THIRD TIME FOR FURTHER TESTING AGAIN AND THEY LATER TOLD THE CONTACT TO PICK UP THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED. THE CONTACT WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER. THE APPROXIMATE FAILURE MILEAGE WAS 365.
Corrective Action:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT STATED THAT THE WARNING INDICATOR ILLUMINATED TO CHECK THE HEAD LAMP SYSTEM AND "SEE MANUAL ON THE DISPLAY" DISPLAYED ON THE MESSAGE BOARD. THE VEHICLE WAS TAKEN TO THE DEALER TWICE, BUT THEY WERE UNABLE TO REPLICATE AND DIAGNOSE THE FAILURE. THE DEALER REPROGRAMMED THE HCM, BUT THE WARNING INDICATOR FLASHED SEVERAL TIMES AGAIN MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER A THIRD TIME FOR FURTHER TESTING AGAIN AND THEY LATER TOLD THE CONTACT TO PICK UP THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED. THE CONTACT WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER. THE APPROXIMATE FAILURE MILEAGE WAS 365.
Additional Notes:
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT STATED THAT THE WARNING INDICATOR ILLUMINATED TO CHECK THE HEAD LAMP SYSTEM AND "SEE MANUAL ON THE DISPLAY" DISPLAYED ON THE MESSAGE BOARD. THE VEHICLE WAS TAKEN TO THE DEALER TWICE, BUT THEY WERE UNABLE TO REPLICATE AND DIAGNOSE THE FAILURE. THE DEALER REPROGRAMMED THE HCM, BUT THE WARNING INDICATOR FLASHED SEVERAL TIMES AGAIN MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER A THIRD TIME FOR FURTHER TESTING AGAIN AND THEY LATER TOLD THE CONTACT TO PICK UP THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED. THE CONTACT WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER. THE APPROXIMATE FAILURE MILEAGE WAS 365.
Mfg Campaign: 10904708
Recall Date: Sep 8, 2016
Need Legal Help?
Featured Attorneys
Barry Edzant
Edzant Price LLC
Valencia, CA • 36 yrs
Focus: Lemon Law, Personal Injury
Recent Articles
Jeep Grand Cherokee Head Restraint Problem
Chrysler (FCA US, LLC) has announced a safety issue affecting certain 2023–2024 Jeep Grand Ch ...
Aug 1, 2025Fuel Injector Problem: 2021-2024 Ford Bronco Sport and 2020-2022 Ford Escape
If you own a 2021-2024 Ford Bronco Sport or 2020-2022 Ford Escape equipped with a 1.5L Dragon GTDI e ...
Jul 28, 2025Airbag Problem Affects 2022-2025 Chrysler Pacifica and Voyager Vehicles
If you own a Chrysler Pacifica or Voyager, your vehicle may be equipped with defective side curtain ...
Jul 24, 2025