Complaints & Recalls
Official Safety Recalls - Important!
4 RecallsThese are official manufacturer recalls ordered by NHTSA for safety defects. If you own this vehicle, contact your dealer immediately for free repairs.
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain 2013-2019 Escape, 2013-2018 C-Max, 2013-2016 Fusion, 2013-2021 Transit Connect, and 2015-2018 Edge vehicles. The bushing that attaches the shifter cable to the transmission may degrade or detach.
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.nhtsa.gov.
Mfg Campaign: 22S43
Recall Date: Jun 10, 2022
Ford Motor Company
Safety Issue:
Ford Motor Company (Ford) is recalling certain model year 2017 Ford Escape Titanium and SE vehicles manufactured October 5, 2015, to May 12, 2016. The settings for the closing-force of the power-operated windows may allow the windows to close on an object such as a body part and injure it before the windows auto-reverse. As such, these vehicles fail to comply with the requirements of Federal Motor Vehicle Safety Standard (FMVSS) number 118, "Power-Operated Window Systems."
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: 16C12
Recall Date: Aug 24, 2016
Consumer Complaints
2.8K ComplaintsFord Motor Company
Defect Description:
ELECTRONIC STABILITY CONTROL (ESC)
Potential Consequences:
UNSTABLE TIRE AND WHEEL,AND STEERING, LOOSE FRONT END SUSPENSION.
Corrective Action:
UNSTABLE TIRE AND WHEEL,AND STEERING, LOOSE FRONT END SUSPENSION.
Additional Notes:
UNSTABLE TIRE AND WHEEL,AND STEERING, LOOSE FRONT END SUSPENSION.
Mfg Campaign: 11073518
Recall Date: Feb 18, 2018
Ford Motor Company
Defect Description:
WHEELS
Potential Consequences:
UNSTABLE TIRE AND WHEEL,AND STEERING, LOOSE FRONT END SUSPENSION.
Corrective Action:
UNSTABLE TIRE AND WHEEL,AND STEERING, LOOSE FRONT END SUSPENSION.
Additional Notes:
UNSTABLE TIRE AND WHEEL,AND STEERING, LOOSE FRONT END SUSPENSION.
Mfg Campaign: 11073518
Recall Date: Feb 18, 2018
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
A MONTH AGO I HAD A CHECK ENGINE LIGHT THAT CAME ON. IT RAN REALLY ROUGH AND FELT LIKE I WAS GOING OVER ROCKS THE WAY THE SUV WAS RUNNING. ON MY PHONE I HAD AN APP THAT SAID THERE WAS A MISFIRE. THEY FIXED IT SAYING THEY REPLACED SOME WIRES. A WEEK AGO THE CHECK ENGINE CAME ON AGAIN. I FELT A BIT OF A JOLT COMING FROM THE ENGINE AS I WAS DRIVING HOME FROM WORK. I DIDNT FIND TIME TIL 2 WEEKS LATER BECAUSE OF MY SCHEDULE.SO I TOOK IT TO A FORD DEALERSHIP TO GET IT FIXED. ON MY WAY THERE, THE COOLANT LEVEL WENT HIGH AND I HAD ANOTHER MISFIRE AGAIN. I FINALLY MADE IT TO THE FORD DEALERSHIP. THEY SEEN THE COOLANT LEAK AND NOTICE THE MISFIRE. THIS FORD ESCAPE IS ONLY 11 MONTHS OLD AND I ALREADY HAD 2 MISFIRE SITUATIONS AND A COOLANT LEAK. I ONLY GO TO WORK AND ONLY DID ONE TRIP TO JOSHUA TREE NATIONAL PARK. IT HAS 23,000 MILES ONLY BECAUSE I HAD TO TRAVEL 30 MILES TO WORK ONE WAY. I FEEL LIKE THIS IS A LEMON SEEING HOW THIS IS THE SECOND TIME FOR THE SAME PROBLEM.
Corrective Action:
A MONTH AGO I HAD A CHECK ENGINE LIGHT THAT CAME ON. IT RAN REALLY ROUGH AND FELT LIKE I WAS GOING OVER ROCKS THE WAY THE SUV WAS RUNNING. ON MY PHONE I HAD AN APP THAT SAID THERE WAS A MISFIRE. THEY FIXED IT SAYING THEY REPLACED SOME WIRES. A WEEK AGO THE CHECK ENGINE CAME ON AGAIN. I FELT A BIT OF A JOLT COMING FROM THE ENGINE AS I WAS DRIVING HOME FROM WORK. I DIDNT FIND TIME TIL 2 WEEKS LATER BECAUSE OF MY SCHEDULE.SO I TOOK IT TO A FORD DEALERSHIP TO GET IT FIXED. ON MY WAY THERE, THE COOLANT LEVEL WENT HIGH AND I HAD ANOTHER MISFIRE AGAIN. I FINALLY MADE IT TO THE FORD DEALERSHIP. THEY SEEN THE COOLANT LEAK AND NOTICE THE MISFIRE. THIS FORD ESCAPE IS ONLY 11 MONTHS OLD AND I ALREADY HAD 2 MISFIRE SITUATIONS AND A COOLANT LEAK. I ONLY GO TO WORK AND ONLY DID ONE TRIP TO JOSHUA TREE NATIONAL PARK. IT HAS 23,000 MILES ONLY BECAUSE I HAD TO TRAVEL 30 MILES TO WORK ONE WAY. I FEEL LIKE THIS IS A LEMON SEEING HOW THIS IS THE SECOND TIME FOR THE SAME PROBLEM.
Additional Notes:
A MONTH AGO I HAD A CHECK ENGINE LIGHT THAT CAME ON. IT RAN REALLY ROUGH AND FELT LIKE I WAS GOING OVER ROCKS THE WAY THE SUV WAS RUNNING. ON MY PHONE I HAD AN APP THAT SAID THERE WAS A MISFIRE. THEY FIXED IT SAYING THEY REPLACED SOME WIRES. A WEEK AGO THE CHECK ENGINE CAME ON AGAIN. I FELT A BIT OF A JOLT COMING FROM THE ENGINE AS I WAS DRIVING HOME FROM WORK. I DIDNT FIND TIME TIL 2 WEEKS LATER BECAUSE OF MY SCHEDULE.SO I TOOK IT TO A FORD DEALERSHIP TO GET IT FIXED. ON MY WAY THERE, THE COOLANT LEVEL WENT HIGH AND I HAD ANOTHER MISFIRE AGAIN. I FINALLY MADE IT TO THE FORD DEALERSHIP. THEY SEEN THE COOLANT LEAK AND NOTICE THE MISFIRE. THIS FORD ESCAPE IS ONLY 11 MONTHS OLD AND I ALREADY HAD 2 MISFIRE SITUATIONS AND A COOLANT LEAK. I ONLY GO TO WORK AND ONLY DID ONE TRIP TO JOSHUA TREE NATIONAL PARK. IT HAS 23,000 MILES ONLY BECAUSE I HAD TO TRAVEL 30 MILES TO WORK ONE WAY. I FEEL LIKE THIS IS A LEMON SEEING HOW THIS IS THE SECOND TIME FOR THE SAME PROBLEM.
Mfg Campaign: 11065984
Recall Date: Jan 31, 2018
Ford Motor Company
Defect Description:
POWER TRAIN
Potential Consequences:
A MONTH AGO I HAD A CHECK ENGINE LIGHT THAT CAME ON. IT RAN REALLY ROUGH AND FELT LIKE I WAS GOING OVER ROCKS THE WAY THE SUV WAS RUNNING. ON MY PHONE I HAD AN APP THAT SAID THERE WAS A MISFIRE. THEY FIXED IT SAYING THEY REPLACED SOME WIRES. A WEEK AGO THE CHECK ENGINE CAME ON AGAIN. I FELT A BIT OF A JOLT COMING FROM THE ENGINE AS I WAS DRIVING HOME FROM WORK. I DIDNT FIND TIME TIL 2 WEEKS LATER BECAUSE OF MY SCHEDULE.SO I TOOK IT TO A FORD DEALERSHIP TO GET IT FIXED. ON MY WAY THERE, THE COOLANT LEVEL WENT HIGH AND I HAD ANOTHER MISFIRE AGAIN. I FINALLY MADE IT TO THE FORD DEALERSHIP. THEY SEEN THE COOLANT LEAK AND NOTICE THE MISFIRE. THIS FORD ESCAPE IS ONLY 11 MONTHS OLD AND I ALREADY HAD 2 MISFIRE SITUATIONS AND A COOLANT LEAK. I ONLY GO TO WORK AND ONLY DID ONE TRIP TO JOSHUA TREE NATIONAL PARK. IT HAS 23,000 MILES ONLY BECAUSE I HAD TO TRAVEL 30 MILES TO WORK ONE WAY. I FEEL LIKE THIS IS A LEMON SEEING HOW THIS IS THE SECOND TIME FOR THE SAME PROBLEM.
Corrective Action:
A MONTH AGO I HAD A CHECK ENGINE LIGHT THAT CAME ON. IT RAN REALLY ROUGH AND FELT LIKE I WAS GOING OVER ROCKS THE WAY THE SUV WAS RUNNING. ON MY PHONE I HAD AN APP THAT SAID THERE WAS A MISFIRE. THEY FIXED IT SAYING THEY REPLACED SOME WIRES. A WEEK AGO THE CHECK ENGINE CAME ON AGAIN. I FELT A BIT OF A JOLT COMING FROM THE ENGINE AS I WAS DRIVING HOME FROM WORK. I DIDNT FIND TIME TIL 2 WEEKS LATER BECAUSE OF MY SCHEDULE.SO I TOOK IT TO A FORD DEALERSHIP TO GET IT FIXED. ON MY WAY THERE, THE COOLANT LEVEL WENT HIGH AND I HAD ANOTHER MISFIRE AGAIN. I FINALLY MADE IT TO THE FORD DEALERSHIP. THEY SEEN THE COOLANT LEAK AND NOTICE THE MISFIRE. THIS FORD ESCAPE IS ONLY 11 MONTHS OLD AND I ALREADY HAD 2 MISFIRE SITUATIONS AND A COOLANT LEAK. I ONLY GO TO WORK AND ONLY DID ONE TRIP TO JOSHUA TREE NATIONAL PARK. IT HAS 23,000 MILES ONLY BECAUSE I HAD TO TRAVEL 30 MILES TO WORK ONE WAY. I FEEL LIKE THIS IS A LEMON SEEING HOW THIS IS THE SECOND TIME FOR THE SAME PROBLEM.
Additional Notes:
A MONTH AGO I HAD A CHECK ENGINE LIGHT THAT CAME ON. IT RAN REALLY ROUGH AND FELT LIKE I WAS GOING OVER ROCKS THE WAY THE SUV WAS RUNNING. ON MY PHONE I HAD AN APP THAT SAID THERE WAS A MISFIRE. THEY FIXED IT SAYING THEY REPLACED SOME WIRES. A WEEK AGO THE CHECK ENGINE CAME ON AGAIN. I FELT A BIT OF A JOLT COMING FROM THE ENGINE AS I WAS DRIVING HOME FROM WORK. I DIDNT FIND TIME TIL 2 WEEKS LATER BECAUSE OF MY SCHEDULE.SO I TOOK IT TO A FORD DEALERSHIP TO GET IT FIXED. ON MY WAY THERE, THE COOLANT LEVEL WENT HIGH AND I HAD ANOTHER MISFIRE AGAIN. I FINALLY MADE IT TO THE FORD DEALERSHIP. THEY SEEN THE COOLANT LEAK AND NOTICE THE MISFIRE. THIS FORD ESCAPE IS ONLY 11 MONTHS OLD AND I ALREADY HAD 2 MISFIRE SITUATIONS AND A COOLANT LEAK. I ONLY GO TO WORK AND ONLY DID ONE TRIP TO JOSHUA TREE NATIONAL PARK. IT HAS 23,000 MILES ONLY BECAUSE I HAD TO TRAVEL 30 MILES TO WORK ONE WAY. I FEEL LIKE THIS IS A LEMON SEEING HOW THIS IS THE SECOND TIME FOR THE SAME PROBLEM.
Mfg Campaign: 11065984
Recall Date: Jan 31, 2018
Ford Motor Company
Defect Description:
POWER TRAIN
Potential Consequences:
TRANSMISSION FAILED AND WAS REBUILT BY ROUTE 23 AUTOMALL. ONCE GETTING IT BACK THE TRANSMISSION INTERMITTENTLY SLIPS OUT OF GEAR OFTEN TIMES AFTER STOPPING AT AN INTERSECTION OR TRAFFIC LIGHT OR DURING CITY DRIVING. NO ERROR CODES WHEN BRING IT BACK TO DEALER. CAR IS UNSAFE AS I ALMOST GOT HIT WHILE CROSSING AN INTERSECTION BECAUSE THE TRANSMISSION SLIPPED OUT OF GEAR. ESCALATED TO THE DEALERSHIP AND FORD AND THEY REFUSE TO FIX IT BECAUSE IT IS INTERMITTENT AND NO CODES SHOWN ON THE COMPUTER.
Corrective Action:
TRANSMISSION FAILED AND WAS REBUILT BY ROUTE 23 AUTOMALL. ONCE GETTING IT BACK THE TRANSMISSION INTERMITTENTLY SLIPS OUT OF GEAR OFTEN TIMES AFTER STOPPING AT AN INTERSECTION OR TRAFFIC LIGHT OR DURING CITY DRIVING. NO ERROR CODES WHEN BRING IT BACK TO DEALER. CAR IS UNSAFE AS I ALMOST GOT HIT WHILE CROSSING AN INTERSECTION BECAUSE THE TRANSMISSION SLIPPED OUT OF GEAR. ESCALATED TO THE DEALERSHIP AND FORD AND THEY REFUSE TO FIX IT BECAUSE IT IS INTERMITTENT AND NO CODES SHOWN ON THE COMPUTER.
Additional Notes:
TRANSMISSION FAILED AND WAS REBUILT BY ROUTE 23 AUTOMALL. ONCE GETTING IT BACK THE TRANSMISSION INTERMITTENTLY SLIPS OUT OF GEAR OFTEN TIMES AFTER STOPPING AT AN INTERSECTION OR TRAFFIC LIGHT OR DURING CITY DRIVING. NO ERROR CODES WHEN BRING IT BACK TO DEALER. CAR IS UNSAFE AS I ALMOST GOT HIT WHILE CROSSING AN INTERSECTION BECAUSE THE TRANSMISSION SLIPPED OUT OF GEAR. ESCALATED TO THE DEALERSHIP AND FORD AND THEY REFUSE TO FIX IT BECAUSE IT IS INTERMITTENT AND NO CODES SHOWN ON THE COMPUTER.
Mfg Campaign: 11065816
Recall Date: Jan 30, 2018
Ford Motor Company
Defect Description:
SERVICE BRAKES
Potential Consequences:
BRAKE PEDAL WOULD GO REAL HARD AND HARDLY STOP THE CAR, THEN IT WOULD BE OK AND EVERY THING WOULD WORK PROPER FOR A FEW DAYS. WHEN AT A STOP LIGHT AND MOTOR TURNS OFF IT SOMETIMES WOULD START UP AGAIN BEFORE YOU LIFTED YOUR FOOT. NO DASH LIGHTS WOULD COME ON SHOWING A PROBLEM, I DONT KNOW IF FAULT CODES WERE STORED. THE VEHICLE IS NOT SAFE TO BE ON THE ROAD.
Corrective Action:
BRAKE PEDAL WOULD GO REAL HARD AND HARDLY STOP THE CAR, THEN IT WOULD BE OK AND EVERY THING WOULD WORK PROPER FOR A FEW DAYS. WHEN AT A STOP LIGHT AND MOTOR TURNS OFF IT SOMETIMES WOULD START UP AGAIN BEFORE YOU LIFTED YOUR FOOT. NO DASH LIGHTS WOULD COME ON SHOWING A PROBLEM, I DONT KNOW IF FAULT CODES WERE STORED. THE VEHICLE IS NOT SAFE TO BE ON THE ROAD.
Additional Notes:
BRAKE PEDAL WOULD GO REAL HARD AND HARDLY STOP THE CAR, THEN IT WOULD BE OK AND EVERY THING WOULD WORK PROPER FOR A FEW DAYS. WHEN AT A STOP LIGHT AND MOTOR TURNS OFF IT SOMETIMES WOULD START UP AGAIN BEFORE YOU LIFTED YOUR FOOT. NO DASH LIGHTS WOULD COME ON SHOWING A PROBLEM, I DONT KNOW IF FAULT CODES WERE STORED. THE VEHICLE IS NOT SAFE TO BE ON THE ROAD.
Mfg Campaign: 11065837
Recall Date: Jan 30, 2018
Ford Motor Company
Defect Description:
SERVICE BRAKES
Potential Consequences:
MY 2017 FORD ESCAPE WITH 18,000 HAD A MASTER BRAKE CYLINDER FAILURE AT 18,000 MILES. THE CAR WAS PARKED OUTSIDE OVER NIGHT IN SINGLE DIGIT TEMPERATURES. WHEN I STARTED TO DRIVE IT THE NEXT DAY ON A RESIDENTIAL STREET THE BRAKE PEDAL WENT TO THE FLOOR THE FIRST TIME I APPLIED THE BRAKES AT A STOP SIGN. THE BRAKES ENGAGED , BUT NOT VERY WELL. THE PROBLEM DID NOT GO AWAY AFTER TRYING SEVERAL MORE BRAKE APPLICATIONS, OR BY PUMPING THE BRAKE PEDAL. THERE WAS NO INDICATION FROM THE CAR'S WARNING SYSTEMS THAT THERE WAS ANY PROBLEM WITH THE BRAKE SYSTEM. THE FORD PASS APP ON MY PHONE DIDN'T REPORT ANY PROBLEM EITHER. THE TOTAL LACK OF WARNING IS A REAL CONCERN. THE PROBLEM DID NOT GO AWAY AFTER THE CAR WAS PARKED IN A WARMER GARAGE. I TOOK THE CAR TO THE DEALER AND THEY CONFIRMED THE PROBLEM WAS A FAILED MASTER BRAKE CYLINDER. THEY COULDN'T TELL ME WHAT CAUSED THE FAILURE OR WHAT FAILED. THEY DID SAY THE FAULTY BRAKE CYLINDER WOULD BE SENT TO FORD FOR ANALYSIS. THIS BRAKE SYSTEM FAILURE IS A REAL CONCERN. IN OVER 50 YEARS OF DRIVING I HAVE NEVER HAD A BRAKE MASTER CYLINDER FAIL ON A CAR WITH SUCH LOW MILES. WITHOUT KNOWING WHY IT FAILED I AM CONCERNED THAT IT COULD HAPPEN AGAIN WITH THE REPLACEMENT BRAKE MASTER CYLINDER. NEXT TIME IT COULD HAPPEN AS I AM DRIVING THE CAR AT HIGHER SPEED, OR IN TRAFFIC RESULTING IN AN ACCIDENT. THIS TYPE OF BRAKE SYSTEM FAILURE SHOULD NOT HAPPEN ON ANY NEWER CAR, AND THE CAR'S WARNING SYSTEMS SHOULD BE ABLE LET YOU KNOW THERE IS A PROBLEM WITH ANY PART OF THE BRAKE SYSTEM.
Corrective Action:
MY 2017 FORD ESCAPE WITH 18,000 HAD A MASTER BRAKE CYLINDER FAILURE AT 18,000 MILES. THE CAR WAS PARKED OUTSIDE OVER NIGHT IN SINGLE DIGIT TEMPERATURES. WHEN I STARTED TO DRIVE IT THE NEXT DAY ON A RESIDENTIAL STREET THE BRAKE PEDAL WENT TO THE FLOOR THE FIRST TIME I APPLIED THE BRAKES AT A STOP SIGN. THE BRAKES ENGAGED , BUT NOT VERY WELL. THE PROBLEM DID NOT GO AWAY AFTER TRYING SEVERAL MORE BRAKE APPLICATIONS, OR BY PUMPING THE BRAKE PEDAL. THERE WAS NO INDICATION FROM THE CAR'S WARNING SYSTEMS THAT THERE WAS ANY PROBLEM WITH THE BRAKE SYSTEM. THE FORD PASS APP ON MY PHONE DIDN'T REPORT ANY PROBLEM EITHER. THE TOTAL LACK OF WARNING IS A REAL CONCERN. THE PROBLEM DID NOT GO AWAY AFTER THE CAR WAS PARKED IN A WARMER GARAGE. I TOOK THE CAR TO THE DEALER AND THEY CONFIRMED THE PROBLEM WAS A FAILED MASTER BRAKE CYLINDER. THEY COULDN'T TELL ME WHAT CAUSED THE FAILURE OR WHAT FAILED. THEY DID SAY THE FAULTY BRAKE CYLINDER WOULD BE SENT TO FORD FOR ANALYSIS. THIS BRAKE SYSTEM FAILURE IS A REAL CONCERN. IN OVER 50 YEARS OF DRIVING I HAVE NEVER HAD A BRAKE MASTER CYLINDER FAIL ON A CAR WITH SUCH LOW MILES. WITHOUT KNOWING WHY IT FAILED I AM CONCERNED THAT IT COULD HAPPEN AGAIN WITH THE REPLACEMENT BRAKE MASTER CYLINDER. NEXT TIME IT COULD HAPPEN AS I AM DRIVING THE CAR AT HIGHER SPEED, OR IN TRAFFIC RESULTING IN AN ACCIDENT. THIS TYPE OF BRAKE SYSTEM FAILURE SHOULD NOT HAPPEN ON ANY NEWER CAR, AND THE CAR'S WARNING SYSTEMS SHOULD BE ABLE LET YOU KNOW THERE IS A PROBLEM WITH ANY PART OF THE BRAKE SYSTEM.
Additional Notes:
MY 2017 FORD ESCAPE WITH 18,000 HAD A MASTER BRAKE CYLINDER FAILURE AT 18,000 MILES. THE CAR WAS PARKED OUTSIDE OVER NIGHT IN SINGLE DIGIT TEMPERATURES. WHEN I STARTED TO DRIVE IT THE NEXT DAY ON A RESIDENTIAL STREET THE BRAKE PEDAL WENT TO THE FLOOR THE FIRST TIME I APPLIED THE BRAKES AT A STOP SIGN. THE BRAKES ENGAGED , BUT NOT VERY WELL. THE PROBLEM DID NOT GO AWAY AFTER TRYING SEVERAL MORE BRAKE APPLICATIONS, OR BY PUMPING THE BRAKE PEDAL. THERE WAS NO INDICATION FROM THE CAR'S WARNING SYSTEMS THAT THERE WAS ANY PROBLEM WITH THE BRAKE SYSTEM. THE FORD PASS APP ON MY PHONE DIDN'T REPORT ANY PROBLEM EITHER. THE TOTAL LACK OF WARNING IS A REAL CONCERN. THE PROBLEM DID NOT GO AWAY AFTER THE CAR WAS PARKED IN A WARMER GARAGE. I TOOK THE CAR TO THE DEALER AND THEY CONFIRMED THE PROBLEM WAS A FAILED MASTER BRAKE CYLINDER. THEY COULDN'T TELL ME WHAT CAUSED THE FAILURE OR WHAT FAILED. THEY DID SAY THE FAULTY BRAKE CYLINDER WOULD BE SENT TO FORD FOR ANALYSIS. THIS BRAKE SYSTEM FAILURE IS A REAL CONCERN. IN OVER 50 YEARS OF DRIVING I HAVE NEVER HAD A BRAKE MASTER CYLINDER FAIL ON A CAR WITH SUCH LOW MILES. WITHOUT KNOWING WHY IT FAILED I AM CONCERNED THAT IT COULD HAPPEN AGAIN WITH THE REPLACEMENT BRAKE MASTER CYLINDER. NEXT TIME IT COULD HAPPEN AS I AM DRIVING THE CAR AT HIGHER SPEED, OR IN TRAFFIC RESULTING IN AN ACCIDENT. THIS TYPE OF BRAKE SYSTEM FAILURE SHOULD NOT HAPPEN ON ANY NEWER CAR, AND THE CAR'S WARNING SYSTEMS SHOULD BE ABLE LET YOU KNOW THERE IS A PROBLEM WITH ANY PART OF THE BRAKE SYSTEM.
Mfg Campaign: 11065538
Recall Date: Jan 28, 2018
Ford Motor Company
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Corrective Action:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Additional Notes:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Mfg Campaign: 11064618
Recall Date: Jan 24, 2018
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Corrective Action:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Additional Notes:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Mfg Campaign: 11064618
Recall Date: Jan 24, 2018
Ford Motor Company
Defect Description:
POWER TRAIN
Potential Consequences:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Corrective Action:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Additional Notes:
VEHICLE WENT INTO LIMP MODE WITH NO THROTTLE RESPONSE THE FIRST DAY I OWNED IT. IT LEFT ME ON INTERSTATE I 90 HAVING TO SHUT THE CAR OFF AND TRY TO RESTART IT. THE DEALER COULD NOT FIX THE PROBLEM IT HAPPENED 4 TIMES IN 12K MILES I RETURNED THE VEHICLE TO THE DEALER AS THEY COULD NOT FIND THE PROBLEM AFTER REPLACING SEVERAL DEFECTIVE ELECTRONIC PARTS. THIS VEHICLE WAS GOING TO GET SOMEONE KILLED IT WAS NOT GOING TO BE ME AND MY 14 YEAR OD SON. I UNDERSTAND THAT THEY HAVE AUCTIONED THIS VEHICLE OFF AFTER DISMISSING THE SAFETY CONCERNS. THIS IS THE SECOND REPORT I HAVE FILED ON THIS WEBSITE.
Mfg Campaign: 11064618
Recall Date: Jan 24, 2018
Ford Motor Company
Defect Description:
UNKNOWN OR OTHER
Potential Consequences:
THERE ARE A LOT OF FUMES AND SMELLS GETTING IN SIDE WE HAVE TO ROLL ARE WINDOWS DOWN
Corrective Action:
THERE ARE A LOT OF FUMES AND SMELLS GETTING IN SIDE WE HAVE TO ROLL ARE WINDOWS DOWN
Additional Notes:
THERE ARE A LOT OF FUMES AND SMELLS GETTING IN SIDE WE HAVE TO ROLL ARE WINDOWS DOWN
Mfg Campaign: 11063221
Recall Date: Jan 17, 2018
Ford Motor Company
Defect Description:
AIR BAGS
Potential Consequences:
FRONT COLLISION CAR WAS TOTAL LOSS NO AIR BAGS DEPLOYED FRONT SIDE NOTHING. ON FREEWAY GOING WEST 70 MILES PER HOUR WAS CUT OFF WHILE BRAKING RAN INTO BACK OF PARKED FULL SIZE SUV OUT OF GAS IN THE MEDIUM OFF THE FREEWAY.
Corrective Action:
FRONT COLLISION CAR WAS TOTAL LOSS NO AIR BAGS DEPLOYED FRONT SIDE NOTHING. ON FREEWAY GOING WEST 70 MILES PER HOUR WAS CUT OFF WHILE BRAKING RAN INTO BACK OF PARKED FULL SIZE SUV OUT OF GAS IN THE MEDIUM OFF THE FREEWAY.
Additional Notes:
FRONT COLLISION CAR WAS TOTAL LOSS NO AIR BAGS DEPLOYED FRONT SIDE NOTHING. ON FREEWAY GOING WEST 70 MILES PER HOUR WAS CUT OFF WHILE BRAKING RAN INTO BACK OF PARKED FULL SIZE SUV OUT OF GAS IN THE MEDIUM OFF THE FREEWAY.
Mfg Campaign: 11062542
Recall Date: Jan 13, 2018
Ford Motor Company
Defect Description:
STEERING
Potential Consequences:
WHILE DRIVING ON HIGHWAY AT 75 MPH ( THE SPEED LIMIT IS 75) I WANTED TO PASS A TRUCK WHEN THE STEERING GOT REALLY TIGHT, AT THAT SPEED THEIR IS NO TIME FOR PLAN B. I CLIPPED THE BACK LEFT OF THE TRUCK WITH MY RIGHT FRONT, WHICH PUT ME IN A SPIN AND THE CAR ROLLED A COUPLE TIMES. WHICH RESULTED IN A TOTAL LOSS. I WAS RUSHED TO THE EMERGENCY ROOM AND HAD ALL KINDS OF TESTS AND RELEASED THE NEXT DAY. MY INSURANCE CO DOES NOT BELIEVE ME BUT THAT'S WHAT HAPPENED. I READ MANY ARTICLES ABOUT FORD HAVING PROBLEMS WITH PRIOR YEARS OF THERE ELECTRONIC STEERING. BUT ON THE OTHER HAND IF IT WAS NOT FOR FORD SEATBELT AND AIRBAG SYSTEM I WOULD NOT BE HERE TO WRITE THIS ARTICLE.
Corrective Action:
WHILE DRIVING ON HIGHWAY AT 75 MPH ( THE SPEED LIMIT IS 75) I WANTED TO PASS A TRUCK WHEN THE STEERING GOT REALLY TIGHT, AT THAT SPEED THEIR IS NO TIME FOR PLAN B. I CLIPPED THE BACK LEFT OF THE TRUCK WITH MY RIGHT FRONT, WHICH PUT ME IN A SPIN AND THE CAR ROLLED A COUPLE TIMES. WHICH RESULTED IN A TOTAL LOSS. I WAS RUSHED TO THE EMERGENCY ROOM AND HAD ALL KINDS OF TESTS AND RELEASED THE NEXT DAY. MY INSURANCE CO DOES NOT BELIEVE ME BUT THAT'S WHAT HAPPENED. I READ MANY ARTICLES ABOUT FORD HAVING PROBLEMS WITH PRIOR YEARS OF THERE ELECTRONIC STEERING. BUT ON THE OTHER HAND IF IT WAS NOT FOR FORD SEATBELT AND AIRBAG SYSTEM I WOULD NOT BE HERE TO WRITE THIS ARTICLE.
Additional Notes:
WHILE DRIVING ON HIGHWAY AT 75 MPH ( THE SPEED LIMIT IS 75) I WANTED TO PASS A TRUCK WHEN THE STEERING GOT REALLY TIGHT, AT THAT SPEED THEIR IS NO TIME FOR PLAN B. I CLIPPED THE BACK LEFT OF THE TRUCK WITH MY RIGHT FRONT, WHICH PUT ME IN A SPIN AND THE CAR ROLLED A COUPLE TIMES. WHICH RESULTED IN A TOTAL LOSS. I WAS RUSHED TO THE EMERGENCY ROOM AND HAD ALL KINDS OF TESTS AND RELEASED THE NEXT DAY. MY INSURANCE CO DOES NOT BELIEVE ME BUT THAT'S WHAT HAPPENED. I READ MANY ARTICLES ABOUT FORD HAVING PROBLEMS WITH PRIOR YEARS OF THERE ELECTRONIC STEERING. BUT ON THE OTHER HAND IF IT WAS NOT FOR FORD SEATBELT AND AIRBAG SYSTEM I WOULD NOT BE HERE TO WRITE THIS ARTICLE.
Mfg Campaign: 11062469
Recall Date: Jan 12, 2018
Ford Motor Company
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
AS MY BOYFRIEND WAS TURNING THE CORNER AT AN INTERSECTION, THE ENGINE SUDDENLY STOPPED. HE WAS ABLE TO STOP DUE TO HIS LOW SPEED. I REMINDED HIM TO PUT HIS FOOT ON THE BRAKE TO RESTART, AND HE DID THAT AND IT STARTED RIGHT UP. HE DIDN'T DO ANYTHING TO MAKE THE ENGINE STOP. THE ONLY THING THAT WAS HAPPENING AT THAT TIME WAS THAT A TEXT WAS COMING IN ON MY SAMSUNG PHONE, WHICH WAS CHARGING AND CONNECTED VIA BLUETOOTH.
Corrective Action:
AS MY BOYFRIEND WAS TURNING THE CORNER AT AN INTERSECTION, THE ENGINE SUDDENLY STOPPED. HE WAS ABLE TO STOP DUE TO HIS LOW SPEED. I REMINDED HIM TO PUT HIS FOOT ON THE BRAKE TO RESTART, AND HE DID THAT AND IT STARTED RIGHT UP. HE DIDN'T DO ANYTHING TO MAKE THE ENGINE STOP. THE ONLY THING THAT WAS HAPPENING AT THAT TIME WAS THAT A TEXT WAS COMING IN ON MY SAMSUNG PHONE, WHICH WAS CHARGING AND CONNECTED VIA BLUETOOTH.
Additional Notes:
AS MY BOYFRIEND WAS TURNING THE CORNER AT AN INTERSECTION, THE ENGINE SUDDENLY STOPPED. HE WAS ABLE TO STOP DUE TO HIS LOW SPEED. I REMINDED HIM TO PUT HIS FOOT ON THE BRAKE TO RESTART, AND HE DID THAT AND IT STARTED RIGHT UP. HE DIDN'T DO ANYTHING TO MAKE THE ENGINE STOP. THE ONLY THING THAT WAS HAPPENING AT THAT TIME WAS THAT A TEXT WAS COMING IN ON MY SAMSUNG PHONE, WHICH WAS CHARGING AND CONNECTED VIA BLUETOOTH.
Mfg Campaign: 11057699
Recall Date: Dec 30, 2017
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
AS MY BOYFRIEND WAS TURNING THE CORNER AT AN INTERSECTION, THE ENGINE SUDDENLY STOPPED. HE WAS ABLE TO STOP DUE TO HIS LOW SPEED. I REMINDED HIM TO PUT HIS FOOT ON THE BRAKE TO RESTART, AND HE DID THAT AND IT STARTED RIGHT UP. HE DIDN'T DO ANYTHING TO MAKE THE ENGINE STOP. THE ONLY THING THAT WAS HAPPENING AT THAT TIME WAS THAT A TEXT WAS COMING IN ON MY SAMSUNG PHONE, WHICH WAS CHARGING AND CONNECTED VIA BLUETOOTH.
Corrective Action:
AS MY BOYFRIEND WAS TURNING THE CORNER AT AN INTERSECTION, THE ENGINE SUDDENLY STOPPED. HE WAS ABLE TO STOP DUE TO HIS LOW SPEED. I REMINDED HIM TO PUT HIS FOOT ON THE BRAKE TO RESTART, AND HE DID THAT AND IT STARTED RIGHT UP. HE DIDN'T DO ANYTHING TO MAKE THE ENGINE STOP. THE ONLY THING THAT WAS HAPPENING AT THAT TIME WAS THAT A TEXT WAS COMING IN ON MY SAMSUNG PHONE, WHICH WAS CHARGING AND CONNECTED VIA BLUETOOTH.
Additional Notes:
AS MY BOYFRIEND WAS TURNING THE CORNER AT AN INTERSECTION, THE ENGINE SUDDENLY STOPPED. HE WAS ABLE TO STOP DUE TO HIS LOW SPEED. I REMINDED HIM TO PUT HIS FOOT ON THE BRAKE TO RESTART, AND HE DID THAT AND IT STARTED RIGHT UP. HE DIDN'T DO ANYTHING TO MAKE THE ENGINE STOP. THE ONLY THING THAT WAS HAPPENING AT THAT TIME WAS THAT A TEXT WAS COMING IN ON MY SAMSUNG PHONE, WHICH WAS CHARGING AND CONNECTED VIA BLUETOOTH.
Mfg Campaign: 11057699
Recall Date: Dec 30, 2017
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Corrective Action:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Additional Notes:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Mfg Campaign: 11057372
Recall Date: Dec 29, 2017
Ford Motor Company
Defect Description:
VEHICLE SPEED CONTROL
Potential Consequences:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Corrective Action:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Additional Notes:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Mfg Campaign: 11057372
Recall Date: Dec 29, 2017
Ford Motor Company
Defect Description:
ENGINE
Potential Consequences:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Corrective Action:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Additional Notes:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Mfg Campaign: 11057381
Recall Date: Dec 29, 2017
Ford Motor Company
Defect Description:
VEHICLE SPEED CONTROL
Potential Consequences:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Corrective Action:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Additional Notes:
I TURNED FROM THE PARKING LOT INTERSECTION IN EAGLE RUN SHOPPING CENTER, NW OF WENDY'S, FROM WEST TO SOUTH ONTO THE PARKING LOT ROAD THAT ACCESSES THE W MAPLE RD & BIRCH ST INTERSECTION. I COMPLETED MY TURN AND DROVE SOUTH DOWN THE PARKING LOT ACCESS ROAD TO THE W MAPLE & BIRCH ST INTERSECTION WHERE THE TRAFFIC LIGHT WAS RED. I CAME TO A COMPLETE STOP TO WAIT FOR A GREEN LIGHT. I STOPPED A WAYS BACK FROM THE MEDIAN CURB OF THE INTERSECTION TO ALLOW FOR TURNING TRAFFIC FROM THE WEST. SHORTLY LATER, WHILE WAITING FOR THE LIGHT TO CHANGE, I NOTICED A VIBRATION OF THE CAR AND LOOKED AT THE TACHOMETER WHICH SHOWED 1,200 RPM & RISING (600RPM IS NORMAL). IMMEDIATELY THE CAR BEGAN TO PHYSICALLY LUNGE FORWARD WITH INCREASED ENGINE NOISE SO I INSTINCTIVELY PLACED MORE PRESSURE ON THE BRAKE PEDAL WHICH HAD NO AFFECT. THE CAR'S ENGINE WAS NOW RACING WIDE OPEN & I HAD NO CONTROL OF THE CAR'S RAPIDLY INCREASING FORWARD MOTION. AT THIS POINT, TO AVOID A CATASTROPHIC ACCIDENT BY BEING PULLED INTO TRAFFIC AT THE INTERSECTION, I STEERED TO THE RIGHT TOWARDS THE SHOULDER HITTING THE TRAFFIC LIGHT POLE WITH THE BRAKE APPLIED THE ENTIRE TIME.
Mfg Campaign: 11057381
Recall Date: Dec 29, 2017
Ford Motor Company
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
THE VEHICLE WAS PARKED AND WOULD NOT TURN ON. LIGHTS AND RADIO WORKED BUT ENGINE WOULD NOT. ELECTRONIC CONTROL MODULE WAS REPLACED. TWO WEEKS AFTER PICKING IT UP FROM THE DEALER SAME THING HAPPENED WHEN IT WAS PARKED. NEXT DAY THE CAR WOULD TURN ON. TRIED TO TURN IT ON AGAIN 15 MINUTES LATER IT WOULD NOT TURN ON. HAD IT TOWED TO THE DEALER. ELECTRONIC CONTROL MODULE REPLACED AGAIN. ONE MONTH LATER SAME THING HAPPENED WHILE PARKED. CALLED FOR TOW TRUCK TO HAVE IT TOWED. WHILE WAITING FOR THE TOW TRUCK AFTER 2 HOURS TRIED TURNING IT ON AND IT DID TURN ON. STILL HAD IT TOWED TO THE DEALER.
Corrective Action:
THE VEHICLE WAS PARKED AND WOULD NOT TURN ON. LIGHTS AND RADIO WORKED BUT ENGINE WOULD NOT. ELECTRONIC CONTROL MODULE WAS REPLACED. TWO WEEKS AFTER PICKING IT UP FROM THE DEALER SAME THING HAPPENED WHEN IT WAS PARKED. NEXT DAY THE CAR WOULD TURN ON. TRIED TO TURN IT ON AGAIN 15 MINUTES LATER IT WOULD NOT TURN ON. HAD IT TOWED TO THE DEALER. ELECTRONIC CONTROL MODULE REPLACED AGAIN. ONE MONTH LATER SAME THING HAPPENED WHILE PARKED. CALLED FOR TOW TRUCK TO HAVE IT TOWED. WHILE WAITING FOR THE TOW TRUCK AFTER 2 HOURS TRIED TURNING IT ON AND IT DID TURN ON. STILL HAD IT TOWED TO THE DEALER.
Additional Notes:
THE VEHICLE WAS PARKED AND WOULD NOT TURN ON. LIGHTS AND RADIO WORKED BUT ENGINE WOULD NOT. ELECTRONIC CONTROL MODULE WAS REPLACED. TWO WEEKS AFTER PICKING IT UP FROM THE DEALER SAME THING HAPPENED WHEN IT WAS PARKED. NEXT DAY THE CAR WOULD TURN ON. TRIED TO TURN IT ON AGAIN 15 MINUTES LATER IT WOULD NOT TURN ON. HAD IT TOWED TO THE DEALER. ELECTRONIC CONTROL MODULE REPLACED AGAIN. ONE MONTH LATER SAME THING HAPPENED WHILE PARKED. CALLED FOR TOW TRUCK TO HAVE IT TOWED. WHILE WAITING FOR THE TOW TRUCK AFTER 2 HOURS TRIED TURNING IT ON AND IT DID TURN ON. STILL HAD IT TOWED TO THE DEALER.
Mfg Campaign: 11056268
Recall Date: Dec 24, 2017
Need Legal Help?
Featured Attorneys
Barry Edzant
Edzant Price LLC
Valencia, CA • 36 yrs
Focus: Lemon Law, Personal Injury